37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 324917 |
Time | |
Date | 199601 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : clt |
State Reference | NC |
Altitude | msl bound lower : 750 msl bound upper : 4000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : clt tower : clt |
Operator | common carrier : air carrier |
Make Model Name | DC-9 30 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 10000 flight time type : 3600 |
ASRS Report | 324917 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other controllera other flight crewa |
Resolutory Action | flight crew : declared emergency other other |
Consequence | other Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
During takeoff at vr, 143 KTS, we began rotation, felt a vibration followed by a bang. Aircraft became airborne normally, flight controls and engines normal. Right main gear green down lock light was out, red 'gear unsafe' light on. We did not attempt to retract gear, went to departure control, leveled off at 4000 ft and began a vector for an extended pattern back to the airport. We performed all abnormal procedures including viewing the landing gear through viewing port in cabin floor. Gear indicated locked down, the tires could not be observed, however, wire conduits could be seen broken, gear doors appeared normal. Tower confirmed the remains of #1 tire were found on the runway. Flight attendants were briefed and passenger also for emergency landing. Landing was uneventful. #3 tire had blown and stripped off rubber. #4 tire was in good shape. Wiring to gear switch was gone and a hole in flap approximately 12 inches on trailing edge. No apparent engine FOD ingestion was noted. Crew performance was excellent. Coordination and communications between cockpit, cabin crew, and passenger was maintained. Good CRM.
Original NASA ASRS Text
Title: FLC OF AN MLG DECLARED AN EMER AND RETURNED TO LAND AFTER AN UNSAFE MAIN GEAR LIGHT DUE TO A DAMAGED LNDG GEAR CAUSED BY A BLOWN TIRE ON TKOF.
Narrative: DURING TKOF AT VR, 143 KTS, WE BEGAN ROTATION, FELT A VIBRATION FOLLOWED BY A BANG. ACFT BECAME AIRBORNE NORMALLY, FLT CTLS AND ENGS NORMAL. R MAIN GEAR GREEN DOWN LOCK LIGHT WAS OUT, RED 'GEAR UNSAFE' LIGHT ON. WE DID NOT ATTEMPT TO RETRACT GEAR, WENT TO DEP CTL, LEVELED OFF AT 4000 FT AND BEGAN A VECTOR FOR AN EXTENDED PATTERN BACK TO THE ARPT. WE PERFORMED ALL ABNORMAL PROCS INCLUDING VIEWING THE LNDG GEAR THROUGH VIEWING PORT IN CABIN FLOOR. GEAR INDICATED LOCKED DOWN, THE TIRES COULD NOT BE OBSERVED, HOWEVER, WIRE CONDUITS COULD BE SEEN BROKEN, GEAR DOORS APPEARED NORMAL. TWR CONFIRMED THE REMAINS OF #1 TIRE WERE FOUND ON THE RWY. FLT ATTENDANTS WERE BRIEFED AND PAX ALSO FOR EMER LNDG. LNDG WAS UNEVENTFUL. #3 TIRE HAD BLOWN AND STRIPPED OFF RUBBER. #4 TIRE WAS IN GOOD SHAPE. WIRING TO GEAR SWITCH WAS GONE AND A HOLE IN FLAP APPROX 12 INCHES ON TRAILING EDGE. NO APPARENT ENG FOD INGESTION WAS NOTED. CREW PERFORMANCE WAS EXCELLENT. COORD AND COMS BTWN COCKPIT, CABIN CREW, AND PAX WAS MAINTAINED. GOOD CRM.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.