37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 332893 |
Time | |
Date | 199604 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : tpa |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-400 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 255 flight time total : 25000 flight time type : 3700 |
ASRS Report | 332893 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On entering jetway noticed strong petro/chemical odor down jetway and throughout aircraft cabin. There was no evidence of fuel spill outside and maintenance explanation ranged from conditioned air from the terminal, to bug spray. Since I couldn't get substantiation for the bug spray theory I elected to not accept the aircraft. We had an MEL on an auxiliary fuel tank that on investigation by maintenance had an internal fuel leak. Apparently the fueler pumped fuel by mistake into the tank without telling anyone. The strongly voiced concern from the cabin crew significantly contributed to a safe conclusion. CRM strikes again. Callback conversation with reporter revealed the following information: the reporter was flying a B737-400 at the time of the incident. This aircraft had an MEL restr that prevented use of the center fuel tank, but did not explain the reason why. The reporter said that he had just finished a walkaround inspection and during this he had noted fuel dripping from a fuselage drain. He then entered the aircraft and noted fuel odors in the jetway and the flight station. The flight attendants complained of the fuel smell in the cabin while he was reviewing the maintenance log. He then called for maintenance assistance on the radio. The maintenance technicians came up with a number of reasons for the smell that were unsatisfactory to the flight crew and the flight attendants so the captain called a maintenance supervisor. The supervisor discovered that the center tank had an in-the-aircraft leak and was not supposed to be fueled. However, a fueler had apparently put some fuel in the tank in the recent past. The aircraft was taken OTS. The reporter said that he wanted to emphasize the flight attendants' role as advocates during this event. He said that their strong stand pushed him to contact the supervisor for more information and the supervisor found out about the misfueling.
Original NASA ASRS Text
Title: AN ACR FLC FINDS THAT THEIR ACFT HAD FUEL IN THE CTR TANK EVEN THOUGH IT WAS MEL'D AS UNUSABLE BECAUSE OF AN INTERNAL FUEL LEAK.
Narrative: ON ENTERING JETWAY NOTICED STRONG PETRO/CHEMICAL ODOR DOWN JETWAY AND THROUGHOUT ACFT CABIN. THERE WAS NO EVIDENCE OF FUEL SPILL OUTSIDE AND MAINT EXPLANATION RANGED FROM CONDITIONED AIR FROM THE TERMINAL, TO BUG SPRAY. SINCE I COULDN'T GET SUBSTANTIATION FOR THE BUG SPRAY THEORY I ELECTED TO NOT ACCEPT THE ACFT. WE HAD AN MEL ON AN AUX FUEL TANK THAT ON INVESTIGATION BY MAINT HAD AN INTERNAL FUEL LEAK. APPARENTLY THE FUELER PUMPED FUEL BY MISTAKE INTO THE TANK WITHOUT TELLING ANYONE. THE STRONGLY VOICED CONCERN FROM THE CABIN CREW SIGNIFICANTLY CONTRIBUTED TO A SAFE CONCLUSION. CRM STRIKES AGAIN. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR WAS FLYING A B737-400 AT THE TIME OF THE INCIDENT. THIS ACFT HAD AN MEL RESTR THAT PREVENTED USE OF THE CTR FUEL TANK, BUT DID NOT EXPLAIN THE REASON WHY. THE RPTR SAID THAT HE HAD JUST FINISHED A WALKAROUND INSPECTION AND DURING THIS HE HAD NOTED FUEL DRIPPING FROM A FUSELAGE DRAIN. HE THEN ENTERED THE ACFT AND NOTED FUEL ODORS IN THE JETWAY AND THE FLT STATION. THE FLT ATTENDANTS COMPLAINED OF THE FUEL SMELL IN THE CABIN WHILE HE WAS REVIEWING THE MAINT LOG. HE THEN CALLED FOR MAINT ASSISTANCE ON THE RADIO. THE MAINT TECHNICIANS CAME UP WITH A NUMBER OF REASONS FOR THE SMELL THAT WERE UNSATISFACTORY TO THE FLC AND THE FLT ATTENDANTS SO THE CAPT CALLED A MAINT SUPVR. THE SUPVR DISCOVERED THAT THE CTR TANK HAD AN IN-THE-ACFT LEAK AND WAS NOT SUPPOSED TO BE FUELED. HOWEVER, A FUELER HAD APPARENTLY PUT SOME FUEL IN THE TANK IN THE RECENT PAST. THE ACFT WAS TAKEN OTS. THE RPTR SAID THAT HE WANTED TO EMPHASIZE THE FLT ATTENDANTS' ROLE AS ADVOCATES DURING THIS EVENT. HE SAID THAT THEIR STRONG STAND PUSHED HIM TO CONTACT THE SUPVR FOR MORE INFO AND THE SUPVR FOUND OUT ABOUT THE MISFUELING.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.