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|
Attributes | |
ACN | 335755 |
Time | |
Date | 199605 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dca airport : bwi |
State Reference | DC |
Altitude | msl bound lower : 1500 msl bound upper : 1500 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : dca |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | descent : approach landing : missed approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | other other : other pilot : atp pilot : flight engineer pilot : instrument |
Experience | flight time last 90 days : 166 flight time total : 12750 flight time type : 4500 |
ASRS Report | 335755 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : overcame equipment problem other other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
During approach to dca, landing gear was extended for landing. Landing gear position lights were inoperative so no positive down and locked indication was observed. A missed approach was made, a manual gear extension and visual confirmation of the gear being down and locked was performed. Flight was diverted to bwi which had better WX and a longer runway. Landing was uneventful.
Original NASA ASRS Text
Title: FLC OF A B737-300 MADE A MISSED APCH AND DIVERTED TO LAND AFTER THE LNDG GEAR DOWN LIGHTS DID NOT LIGHT WITH THE GEAR DOWN.
Narrative: DURING APCH TO DCA, LNDG GEAR WAS EXTENDED FOR LNDG. LNDG GEAR POS LIGHTS WERE INOP SO NO POSITIVE DOWN AND LOCKED INDICATION WAS OBSERVED. A MISSED APCH WAS MADE, A MANUAL GEAR EXTENSION AND VISUAL CONFIRMATION OF THE GEAR BEING DOWN AND LOCKED WAS PERFORMED. FLT WAS DIVERTED TO BWI WHICH HAD BETTER WX AND A LONGER RWY. LNDG WAS UNEVENTFUL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.