37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 341381 |
Time | |
Date | 199607 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : bos |
State Reference | MA |
Altitude | agl bound lower : 0 agl bound upper : 8000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : bos tower : fay |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude cruise other ground other : taxi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 341381 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
During taxi, captain shut down the left pack due to an unrelated problem. Left pack switch was off, isolation valve was closed. Right bleed switch was on. After takeoff, aircraft would not pressurize. Climb rate was slowed and aircraft leveled off at 8000 ft MSL. Pressurization could not be restored in automatic, standby, or manual modes. It was noted that the outflow valve was closed and right duct pressure was 30 psi, yet cabin climbed and descended with the aircraft. A check for air leaks or structural damage was accomplished. None were noted. Captain elected to continue unpressurized at 10000 ft to bwi. FMC determined en route and reserve fuel to be within limits.
Original NASA ASRS Text
Title: AN ACR MLG FLEW UNPRESSURIZED BOS-BWI BECAUSE THE CREW COULD NOT GET THE PRESSURIZATION SYS TO WORK. ACFT EQUIP PROB PRESSURIZATION SYS.
Narrative: DURING TAXI, CAPT SHUT DOWN THE L PACK DUE TO AN UNRELATED PROB. L PACK SWITCH WAS OFF, ISOLATION VALVE WAS CLOSED. R BLEED SWITCH WAS ON. AFTER TKOF, ACFT WOULD NOT PRESSURIZE. CLB RATE WAS SLOWED AND ACFT LEVELED OFF AT 8000 FT MSL. PRESSURIZATION COULD NOT BE RESTORED IN AUTO, STANDBY, OR MANUAL MODES. IT WAS NOTED THAT THE OUTFLOW VALVE WAS CLOSED AND R DUCT PRESSURE WAS 30 PSI, YET CABIN CLBED AND DSNDED WITH THE ACFT. A CHK FOR AIR LEAKS OR STRUCTURAL DAMAGE WAS ACCOMPLISHED. NONE WERE NOTED. CAPT ELECTED TO CONTINUE UNPRESSURIZED AT 10000 FT TO BWI. FMC DETERMINED ENRTE AND RESERVE FUEL TO BE WITHIN LIMITS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.