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|
Attributes | |
ACN | 343889 |
Time | |
Date | 199608 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : oxv |
State Reference | IA |
Altitude | msl bound lower : 4500 msl bound upper : 4500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : dsm |
Operator | general aviation : personal |
Make Model Name | Amateur (Home) Built |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise other other other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 20 flight time total : 1740 flight time type : 740 |
ASRS Report | 343889 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | controller : provided flight assist flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Propeller failure, part of 1 blade of wooden propeller broke off caused by failure of exhaust system. About 6 inches of right exhaust pipe was missing. I think that exhaust pipe piece broke off, went through propeller arc, striking propeller causing a fracture which rapidly grew causing about 1/3 of 1 propeller blade to depart. We were in cruise flight en route GPS direct from cedar rapids to hutchinson at 4500 ft MSL. I was monitoring dsm approach since we would pass just south of their airspace. About 12 mi east of knoxville we experienced a vibration which quickly became very severe. I closed the throttles, moved mixture to idle cutoff and switched off magnetos. I pulled up to bleed off airspeed to get the propeller stopped. This happened at 58 KIAS. Established best glide and contacted dsm approach for vectors to nearest airport. They established radar contact and gave me a vector to knoxville airport. It became apparent we could not reach the airport so looked for possible sites and selected a portion of highway 92. Made a right pattern and landed about 10 mi east of knoxville. No damage to aircraft or ground vehicles or people. Removed aircraft to knoxville airport for repair.
Original NASA ASRS Text
Title: EXPERIMENTAL HOMEBUILT WITH PUSHER PROP HAD A SMALL PORTION OF EXHAUST SYS BREAK OFF AND IT PASSED THROUGH PROP, CAUSING PROP BLADE FAILURE.
Narrative: PROP FAILURE, PART OF 1 BLADE OF WOODEN PROP BROKE OFF CAUSED BY FAILURE OF EXHAUST SYS. ABOUT 6 INCHES OF R EXHAUST PIPE WAS MISSING. I THINK THAT EXHAUST PIPE PIECE BROKE OFF, WENT THROUGH PROP ARC, STRIKING PROP CAUSING A FRACTURE WHICH RAPIDLY GREW CAUSING ABOUT 1/3 OF 1 PROP BLADE TO DEPART. WE WERE IN CRUISE FLT ENRTE GPS DIRECT FROM CEDAR RAPIDS TO HUTCHINSON AT 4500 FT MSL. I WAS MONITORING DSM APCH SINCE WE WOULD PASS JUST S OF THEIR AIRSPACE. ABOUT 12 MI E OF KNOXVILLE WE EXPERIENCED A VIBRATION WHICH QUICKLY BECAME VERY SEVERE. I CLOSED THE THROTTLES, MOVED MIXTURE TO IDLE CUTOFF AND SWITCHED OFF MAGNETOS. I PULLED UP TO BLEED OFF AIRSPD TO GET THE PROP STOPPED. THIS HAPPENED AT 58 KIAS. ESTABLISHED BEST GLIDE AND CONTACTED DSM APCH FOR VECTORS TO NEAREST ARPT. THEY ESTABLISHED RADAR CONTACT AND GAVE ME A VECTOR TO KNOXVILLE ARPT. IT BECAME APPARENT WE COULD NOT REACH THE ARPT SO LOOKED FOR POSSIBLE SITES AND SELECTED A PORTION OF HWY 92. MADE A R PATTERN AND LANDED ABOUT 10 MI E OF KNOXVILLE. NO DAMAGE TO ACFT OR GND VEHICLES OR PEOPLE. REMOVED ACFT TO KNOXVILLE ARPT FOR REPAIR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.