37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 349291 |
Time | |
Date | 199610 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : atl |
State Reference | GA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B757 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 16000 flight time type : 5000 |
ASRS Report | 349291 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 10000 flight time type : 100 |
ASRS Report | 349310 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | flight crew : rejected takeoff flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
During takeoff cockpit began to fill with smoke. Takeoff was aborted between 110-120 KTS. (V1 was 135 KTS.) flight attendants had some smoke in cabin. Announcement was made to inform attendants of problem and ease passenger concerns,. Brake temperature charts checked. Maintenance advised us to return to atl gate with emergency equipment escort. Supplemental information from acn 349310: aircraft was returned to line after maintenance had washed engines (using chemical cleaners) -- suspect that they did not run-up engines after wash, but who knows? My flight attendant team did a great job in taking control of cabin.
Original NASA ASRS Text
Title: B757 CREW IN A TKOF ABORTED SIT AS SMOKE IS VISIBLE IN COCKPIT DURING TKOF ROLL.
Narrative: DURING TKOF COCKPIT BEGAN TO FILL WITH SMOKE. TKOF WAS ABORTED BTWN 110-120 KTS. (V1 WAS 135 KTS.) FLT ATTENDANTS HAD SOME SMOKE IN CABIN. ANNOUNCEMENT WAS MADE TO INFORM ATTENDANTS OF PROB AND EASE PAX CONCERNS,. BRAKE TEMP CHARTS CHKED. MAINT ADVISED US TO RETURN TO ATL GATE WITH EMER EQUIP ESCORT. SUPPLEMENTAL INFO FROM ACN 349310: ACFT WAS RETURNED TO LINE AFTER MAINT HAD WASHED ENGS (USING CHEMICAL CLEANERS) -- SUSPECT THAT THEY DID NOT RUN-UP ENGS AFTER WASH, BUT WHO KNOWS? MY FLT ATTENDANT TEAM DID A GREAT JOB IN TAKING CTL OF CABIN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.