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|
Attributes | |
ACN | 368411 |
Time | |
Date | 199705 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : pbi |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | ground : preflight |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 368411 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On the exterior inspection, we discovered an apparent previous repair and subsequent damage to #2 engine intake dynarohr lining at the 12 O'clock position. From the ground, an approximately 2 square ft area appeared wrinkled with a crack along the forward rivet line. Contract maintenance was called and the mechanic discovered that the intake had indeed been previously repaired but with an elastic, rubbery compound that he said was no longer authority/authorized for intake repair work. The repair had come loose along the forward edge and the airflow had forced its way under the repair area and had then delaminated the metal surface of the lining from the honeycomb base, from the beginning of the intake towards the aft, almost to the rear of the lining. The lining appeared to be ready to separate and if this were to happen in-flight would have severely damaged the engine and probably would have resulted in an in-flight engine failure or shutdown. Review of the aircraft damage log showed no previous repair work noted for the #2 engine intake. In summary: 2 things concern me: 1) was the previous repair work done utilizing unauthorized materials? 2) why was there no indication of repair work indicated in the aircraft damage log?
Original NASA ASRS Text
Title: MD80S ACFT DURING PREFLT REVEALED AN APPARENT IMPROPER REPAIR OF THE #2 ENG INTAKE LINING. POSSIBLE UNAUTH MATERIAL WAS USED FOR REPAIR AND THE REPAIR WASN'T IN THE ACFT LOGBOOK.
Narrative: ON THE EXTERIOR INSPECTION, WE DISCOVERED AN APPARENT PREVIOUS REPAIR AND SUBSEQUENT DAMAGE TO #2 ENG INTAKE DYNAROHR LINING AT THE 12 O'CLOCK POS. FROM THE GND, AN APPROX 2 SQUARE FT AREA APPEARED WRINKLED WITH A CRACK ALONG THE FORWARD RIVET LINE. CONTRACT MAINT WAS CALLED AND THE MECH DISCOVERED THAT THE INTAKE HAD INDEED BEEN PREVIOUSLY REPAIRED BUT WITH AN ELASTIC, RUBBERY COMPOUND THAT HE SAID WAS NO LONGER AUTH FOR INTAKE REPAIR WORK. THE REPAIR HAD COME LOOSE ALONG THE FORWARD EDGE AND THE AIRFLOW HAD FORCED ITS WAY UNDER THE REPAIR AREA AND HAD THEN DELAMINATED THE METAL SURFACE OF THE LINING FROM THE HONEYCOMB BASE, FROM THE BEGINNING OF THE INTAKE TOWARDS THE AFT, ALMOST TO THE REAR OF THE LINING. THE LINING APPEARED TO BE READY TO SEPARATE AND IF THIS WERE TO HAPPEN INFLT WOULD HAVE SEVERELY DAMAGED THE ENG AND PROBABLY WOULD HAVE RESULTED IN AN INFLT ENG FAILURE OR SHUTDOWN. REVIEW OF THE ACFT DAMAGE LOG SHOWED NO PREVIOUS REPAIR WORK NOTED FOR THE #2 ENG INTAKE. IN SUMMARY: 2 THINGS CONCERN ME: 1) WAS THE PREVIOUS REPAIR WORK DONE UTILIZING UNAUTH MATERIALS? 2) WHY WAS THERE NO INDICATION OF REPAIR WORK INDICATED IN THE ACFT DAMAGE LOG?
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.