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|
Attributes | |
ACN | 398631 |
Time | |
Date | 199804 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | L-1011-1 100/200/250 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 398631 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure other anomaly other |
Independent Detector | other other : unspecified atc other other : unspecified |
Resolutory Action | none taken : detected after the fact other |
Consequence | faa : investigated Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
I performed on the 2L fuel quantity system on apr/xa/98, at approximately XA00 EST. The tank was defueled and sumped. All probes in 2L tank were checked for integrity. As per maintenance coordination the fuel probes, numbers 5 through 9, were replaced along with 2L signal conditioner, then the tank quantity indicators were recalibrated to zero quantity. All maintenance was performed per maintenance manual. The aircraft was then moved to the air carrier tech operations center for a #3 engine change. The aircraft was returned to service on apr/xe/98, approximately 36 hours after fuel tank maintenance was performed. On apr/xc/98, ZZZ tower reported that on takeoff something was streaming from the left outboard wing. Visual inspection noted fuel coming from the top of the wing. Aircraft returned to ZZZ. ZZZ maintenance found missing fasteners at the #5 fuel probe, on the 2L fuel tank. Callback conversation with reporter revealed the following information: the reporter stated the fuel quantity work was accomplished solely by the reporter and is sure all the tank probe covers were torqued to maintenance manual limits. The reporter said the mechanic who repaired the aircraft reported 4 fasteners were missing and one was intact and tight. The reporter stated the FAA has made contact.
Original NASA ASRS Text
Title: AN L1011-100 WAS DISPATCHED WITH A L WING FUEL QUANTITY TANK PROBE COVER PLATE NOT FASTENED.
Narrative: I PERFORMED ON THE 2L FUEL QUANTITY SYS ON APR/XA/98, AT APPROX XA00 EST. THE TANK WAS DEFUELED AND SUMPED. ALL PROBES IN 2L TANK WERE CHKED FOR INTEGRITY. AS PER MAINT COORD THE FUEL PROBES, NUMBERS 5 THROUGH 9, WERE REPLACED ALONG WITH 2L SIGNAL CONDITIONER, THEN THE TANK QUANTITY INDICATORS WERE RECALIBRATED TO ZERO QUANTITY. ALL MAINT WAS PERFORMED PER MAINT MANUAL. THE ACFT WAS THEN MOVED TO THE ACR TECH OPS CTR FOR A #3 ENG CHANGE. THE ACFT WAS RETURNED TO SVC ON APR/XE/98, APPROX 36 HRS AFTER FUEL TANK MAINT WAS PERFORMED. ON APR/XC/98, ZZZ TWR RPTED THAT ON TKOF SOMETHING WAS STREAMING FROM THE L OUTBOARD WING. VISUAL INSPECTION NOTED FUEL COMING FROM THE TOP OF THE WING. ACFT RETURNED TO ZZZ. ZZZ MAINT FOUND MISSING FASTENERS AT THE #5 FUEL PROBE, ON THE 2L FUEL TANK. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE FUEL QUANTITY WORK WAS ACCOMPLISHED SOLELY BY THE RPTR AND IS SURE ALL THE TANK PROBE COVERS WERE TORQUED TO MAINT MANUAL LIMITS. THE RPTR SAID THE MECH WHO REPAIRED THE ACFT RPTED 4 FASTENERS WERE MISSING AND ONE WAS INTACT AND TIGHT. THE RPTR STATED THE FAA HAS MADE CONTACT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.