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|
Attributes | |
ACN | 409527 |
Time | |
Date | 199806 |
Day | Mon |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | A300 |
Operating Under FAR Part | Part 121 |
Flight Phase | other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 409527 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 409526 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | faa : investigated Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On jun/xz/98 I helped change a high pressure bleed valve on #2 engine as per the maintenance manual. Ran up the engine and leak checked as per the maintenance manual. Five days later we were notified that the valve failed. Callback conversation with reporter revealed the following information: the reporter stated the valve that was installed by the reporter checked ok on engine run per the maintenance manual. The reporter said the FAA did investigate this incident and later the company advised the reporter that they were satisfied with the reporter's information and no further action was planned.
Original NASA ASRS Text
Title: AN AIRBUS 300 HAD THE #2 ENG HIGH PRESSURE PNEUMATIC BLEED SHUTOFF VALVE REPLACED AND CHKED PER THE MAINT MANUAL. MECHS WHO REPLACED THE VALVE WERE ADVISED 5 DAYS LATER THAT VALVE HAD FAILED. FAILURE MODE UNKNOWN.
Narrative: ON JUN/XZ/98 I HELPED CHANGE A HIGH PRESSURE BLEED VALVE ON #2 ENG AS PER THE MAINT MANUAL. RAN UP THE ENG AND LEAK CHKED AS PER THE MAINT MANUAL. FIVE DAYS LATER WE WERE NOTIFIED THAT THE VALVE FAILED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE VALVE THAT WAS INSTALLED BY THE RPTR CHKED OK ON ENG RUN PER THE MAINT MANUAL. THE RPTR SAID THE FAA DID INVESTIGATE THIS INCIDENT AND LATER THE COMPANY ADVISED THE RPTR THAT THEY WERE SATISFIED WITH THE RPTR'S INFO AND NO FURTHER ACTION WAS PLANNED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.