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|
Attributes | |
ACN | 412768 |
Time | |
Date | 199808 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : cvg |
State Reference | OH |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 135 |
Navigation In Use | Other |
Flight Phase | ground : preflight other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Experience | flight time last 90 days : 60 flight time total : 1450 flight time type : 60 |
ASRS Report | 412768 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Experience | flight time last 90 days : 105 flight time total : 6800 flight time type : 2090 |
ASRS Report | 413013 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
After takeoff, the nose gear failed to retract. We performed appropriate checklists which called for recycling of the gear. This did not correct the problem and we returned to the airport. On the ground it was discovered that the nose gear pin had broken and the outer sleeve had remained in the nose gear when the central barrel and flag were removed. A maintenance write-up was performed by the captain, the nose gear was inspected and the flight departed again without incident.
Original NASA ASRS Text
Title: A COMMERCIAL FIXED WING LTT ON INITIAL CLB RETURNED TO THE FIELD DUE TO UNABLE TO RETRACT THE NOSE GEAR CAUSED BY A BROKEN NOSE GEAR PIN OUTER SLEEVE REMAINING IN GEAR.
Narrative: AFTER TKOF, THE NOSE GEAR FAILED TO RETRACT. WE PERFORMED APPROPRIATE CHKLISTS WHICH CALLED FOR RECYCLING OF THE GEAR. THIS DID NOT CORRECT THE PROB AND WE RETURNED TO THE ARPT. ON THE GND IT WAS DISCOVERED THAT THE NOSE GEAR PIN HAD BROKEN AND THE OUTER SLEEVE HAD REMAINED IN THE NOSE GEAR WHEN THE CENTRAL BARREL AND FLAG WERE REMOVED. A MAINT WRITE-UP WAS PERFORMED BY THE CAPT, THE NOSE GEAR WAS INSPECTED AND THE FLT DEPARTED AGAIN WITHOUT INCIDENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.