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|
Attributes | |
ACN | 419266 |
Time | |
Date | 199811 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : phx |
State Reference | AZ |
Altitude | agl bound lower : 200 agl bound upper : 200 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : phx |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | climbout : initial climbout : takeoff |
Route In Use | departure other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 190 flight time total : 25475 flight time type : 11500 |
ASRS Report | 419266 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time total : 4936 flight time type : 500 |
ASRS Report | 419376 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | none taken : detected after the fact other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
On takeoff, the landing gear handle would not move past the off position to up. We were doing the abnormal checklist and the pilot on the jump seat noticed the landing gear latch and pressure warning circuit breaker was out. After the reset, the landing gear operation returned to normal, but the red unsafe light was out. I relamped the light. The landing gear was operating normally. After conferring with dispatch and maintenance we continued on our flight to houston, tx. No other problems with the landing gear were noted. The outcome was positive, however, after rethinking the event, I may have used an even safer option.
Original NASA ASRS Text
Title: A B737-500 IMMEDIATELY AFTER TKOF WAS UNABLE TO RAISE THE LNDG GEAR HANDLE TO UP DUE TO THE LEVER LATCH CIRCUIT BREAKER PULLED. RESET CIRCUIT BREAKER AND OP NORMAL.
Narrative: ON TKOF, THE LNDG GEAR HANDLE WOULD NOT MOVE PAST THE OFF POS TO UP. WE WERE DOING THE ABNORMAL CHKLIST AND THE PLT ON THE JUMP SEAT NOTICED THE LNDG GEAR LATCH AND PRESSURE WARNING CIRCUIT BREAKER WAS OUT. AFTER THE RESET, THE LNDG GEAR OP RETURNED TO NORMAL, BUT THE RED UNSAFE LIGHT WAS OUT. I RELAMPED THE LIGHT. THE LNDG GEAR WAS OPERATING NORMALLY. AFTER CONFERRING WITH DISPATCH AND MAINT WE CONTINUED ON OUR FLT TO HOUSTON, TX. NO OTHER PROBS WITH THE LNDG GEAR WERE NOTED. THE OUTCOME WAS POSITIVE, HOWEVER, AFTER RETHINKING THE EVENT, I MAY HAVE USED AN EVEN SAFER OPTION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.