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|
Attributes | |
ACN | 429652 |
Time | |
Date | 199902 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-200 |
Flight Phase | other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 429652 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | none taken : detected after the fact other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
Nose bullet turned loose from #1 engine. Flight diverted due to compressor stalls. Nose bullet was found in the intake with studs attached. It damaged C1 and C2 fans and nose cowl. I was assigned to ship wzx with a #1 engine nose bullet loose. I removed bullet (dome) and installed a new one from stock per maintenance manual procedure. I replaced bullet due to I found some metal debris in old bullet nuts. I determined that there was possible thread wear on the old bullet nut. I inspected the studs on the N1 and N2 case, found secured and in good condition. I installed the new bullet per maintenance manual. After 2 days of flight and 6 legs, it came loose. Callback conversation with reporter revealed the following information: the reporter stated the primary cause of the nose bullet turning loose was the fan case nose cone mounting studs were installed too deeply resulting in inadequate grip length left on the stud. The reporter said the FAA has contacted the air carrier but not the reporter.
Original NASA ASRS Text
Title: A B737-200 DIVERTED DUE TO #1 ENG STALLING CAUSED BY THE NOSE CONE LOOSE IN THE INLET COWL DAMAGING THE C1 AND C2 DISC.
Narrative: NOSE BULLET TURNED LOOSE FROM #1 ENG. FLT DIVERTED DUE TO COMPRESSOR STALLS. NOSE BULLET WAS FOUND IN THE INTAKE WITH STUDS ATTACHED. IT DAMAGED C1 AND C2 FANS AND NOSE COWL. I WAS ASSIGNED TO SHIP WZX WITH A #1 ENG NOSE BULLET LOOSE. I REMOVED BULLET (DOME) AND INSTALLED A NEW ONE FROM STOCK PER MAINT MANUAL PROC. I REPLACED BULLET DUE TO I FOUND SOME METAL DEBRIS IN OLD BULLET NUTS. I DETERMINED THAT THERE WAS POSSIBLE THREAD WEAR ON THE OLD BULLET NUT. I INSPECTED THE STUDS ON THE N1 AND N2 CASE, FOUND SECURED AND IN GOOD CONDITION. I INSTALLED THE NEW BULLET PER MAINT MANUAL. AFTER 2 DAYS OF FLT AND 6 LEGS, IT CAME LOOSE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE PRIMARY CAUSE OF THE NOSE BULLET TURNING LOOSE WAS THE FAN CASE NOSE CONE MOUNTING STUDS WERE INSTALLED TOO DEEPLY RESULTING IN INADEQUATE GRIP LENGTH LEFT ON THE STUD. THE RPTR SAID THE FAA HAS CONTACTED THE ACR BUT NOT THE RPTR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.