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|
Attributes | |
ACN | 437570 |
Time | |
Date | 199905 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : ict.tracon |
State Reference | KS |
Altitude | agl single value : 2000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : ict.tracon |
Operator | general aviation : personal |
Make Model Name | Super King Air 200 HDC |
Flight Phase | climbout : initial |
Route In Use | departure : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : atp |
Experience | flight time last 90 days : 30 flight time total : 11500 flight time type : 200 |
ASRS Report | 437570 |
Person 2 | |
Affiliation | government : faa |
Function | controller : departure |
Qualification | controller : radar |
Events | |
Anomaly | non adherence : clearance other spatial deviation |
Resolutory Action | controller : issued new clearance flight crew : overcame equipment problem |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
This aircraft had just been released from maintenance. Extensive airframe and avionics modification. All ground checks good prior to takeoff, and line-up checks good. After takeoff, #1 HSI heading failed. No flag. Autoplt was engaged about 2000 ft AGL. Aircraft was assigned heading 300 degrees. HSI was set. Actual heading turned out to be approximately 060 degrees as reported by ATC. Remainder of test flight completed using #2 heading and RMI. I do not know anyway that as a single pilot that I could have seen this fault during the 5 mins or so it took from takeoff roll.
Original NASA ASRS Text
Title: A BEECH 35 PLT FAILED TO MAINTAIN ASSIGNED HDG ON DEP FROM ICT.
Narrative: THIS ACFT HAD JUST BEEN RELEASED FROM MAINT. EXTENSIVE AIRFRAME AND AVIONICS MODIFICATION. ALL GND CHKS GOOD PRIOR TO TKOF, AND LINE-UP CHKS GOOD. AFTER TKOF, #1 HSI HDG FAILED. NO FLAG. AUTOPLT WAS ENGAGED ABOUT 2000 FT AGL. ACFT WAS ASSIGNED HDG 300 DEGS. HSI WAS SET. ACTUAL HDG TURNED OUT TO BE APPROX 060 DEGS AS RPTED BY ATC. REMAINDER OF TEST FLT COMPLETED USING #2 HDG AND RMI. I DO NOT KNOW ANYWAY THAT AS A SINGLE PLT THAT I COULD HAVE SEEN THIS FAULT DURING THE 5 MINS OR SO IT TOOK FROM TKOF ROLL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.