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|
Attributes | |
ACN | 439470 |
Time | |
Date | 199906 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
State Reference | TX |
Altitude | msl single value : 6500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zfw.artcc |
Operator | general aviation : personal |
Make Model Name | Skyhawk 172/Cutlass 172 |
Operating Under FAR Part | Part 91 |
Navigation In Use | other vortac |
Flight Phase | cruise : level |
Route In Use | enroute airway : v16.airway |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 25 flight time total : 275 flight time type : 200 |
ASRS Report | 439470 |
Events | |
Anomaly | aircraft equipment problem : less severe |
Independent Detector | other flight crewa |
Resolutory Action | aircraft : equipment problem dissipated flight crew : overcame equipment problem |
Consequence | other |
Factors | |
Maintenance | performance deficiency : repair |
Supplementary | |
Problem Areas | Maintenance Human Performance Flight Crew Human Performance Chart Or Publication Aircraft |
Primary Problem | Maintenance Human Performance |
Situations | |
Publication | Cessna 172RG Pilots Handbook |
Narrative:
A C172RG rental aircraft. Flight was round-trip to el paso direct. About 30 mi west of ink VOR complete radio system lost. All electrical fuses appeared good. Fuel gauges went from reading almost full to about empty. Turning communication master switch off returned fuel gauges to proper reading. Without radios, landing elp was a no-go, did 180 degrees to return to mdd. Feared that used coil installed by FBO had somehow failed. Troubleshooting in-flight next 30 mins failed to resolve. Finally I pulled the alternator fuse switch out, waited 2-3 seconds and pushed back in and communication returned. Resumed flight to elp without further incident. Believe an over-voltage condition caused the alternator control unit to automatically remove alternator field current thus shutting down alternator. Cessna information manual for the cutlass rg model 172RG does not provide emergency procedures for this incident that works. Manual suggests (page 7-32) turning master switch off and on. Communication master switch didn't work. Pulling the alternator fuse switch out and pushing it back in did. My clue was page 3-10 emergency procedures for electrical power supply system 'ammeter indicator discharge' which it did. Step #2 says to check that alternator circuit breaker was in, which it was. I never cycled the engine master switch so don't know if that would have fixed it, most pilots are adverse to turning anything off that has to do with a single-engine plane unless it's on fire. Since the fuse was in and unlike the other 'pop-push to reset type' as it had a tit like it was meant to pull I figured 'what the hell' and pulled it. Nothing happened so I pushed it back in and radios, VOR, transponder all came to life.
Original NASA ASRS Text
Title: C172RG PLT EXPERIENCED ELECTRICAL PROBS INFLT. FINDING PLTS OPERATING HANDBOOK INADEQUATE, USED LOGICAL TROUBLESHOOTING TO RESTORE SYS LOST AND CONTINUED ON.
Narrative: A C172RG RENTAL ACFT. FLT WAS ROUND-TRIP TO EL PASO DIRECT. ABOUT 30 MI W OF INK VOR COMPLETE RADIO SYS LOST. ALL ELECTRICAL FUSES APPEARED GOOD. FUEL GAUGES WENT FROM READING ALMOST FULL TO ABOUT EMPTY. TURNING COM MASTER SWITCH OFF RETURNED FUEL GAUGES TO PROPER READING. WITHOUT RADIOS, LNDG ELP WAS A NO-GO, DID 180 DEGS TO RETURN TO MDD. FEARED THAT USED COIL INSTALLED BY FBO HAD SOMEHOW FAILED. TROUBLESHOOTING INFLT NEXT 30 MINS FAILED TO RESOLVE. FINALLY I PULLED THE ALTERNATOR FUSE SWITCH OUT, WAITED 2-3 SECONDS AND PUSHED BACK IN AND COM RETURNED. RESUMED FLT TO ELP WITHOUT FURTHER INCIDENT. BELIEVE AN OVER-VOLTAGE CONDITION CAUSED THE ALTERNATOR CTL UNIT TO AUTOMATICALLY REMOVE ALTERNATOR FIELD CURRENT THUS SHUTTING DOWN ALTERNATOR. CESSNA INFO MANUAL FOR THE CUTLASS RG MODEL 172RG DOES NOT PROVIDE EMER PROCS FOR THIS INCIDENT THAT WORKS. MANUAL SUGGESTS (PAGE 7-32) TURNING MASTER SWITCH OFF AND ON. COM MASTER SWITCH DIDN'T WORK. PULLING THE ALTERNATOR FUSE SWITCH OUT AND PUSHING IT BACK IN DID. MY CLUE WAS PAGE 3-10 EMER PROCS FOR ELECTRICAL PWR SUPPLY SYS 'AMMETER INDICATOR DISCHARGE' WHICH IT DID. STEP #2 SAYS TO CHK THAT ALTERNATOR CIRCUIT BREAKER WAS IN, WHICH IT WAS. I NEVER CYCLED THE ENG MASTER SWITCH SO DON'T KNOW IF THAT WOULD HAVE FIXED IT, MOST PLTS ARE ADVERSE TO TURNING ANYTHING OFF THAT HAS TO DO WITH A SINGLE-ENG PLANE UNLESS IT'S ON FIRE. SINCE THE FUSE WAS IN AND UNLIKE THE OTHER 'POP-PUSH TO RESET TYPE' AS IT HAD A TIT LIKE IT WAS MEANT TO PULL I FIGURED 'WHAT THE HELL' AND PULLED IT. NOTHING HAPPENED SO I PUSHED IT BACK IN AND RADIOS, VOR, XPONDER ALL CAME TO LIFE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.