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|
Attributes | |
ACN | 457067 |
Time | |
Date | 199911 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : rdu.airport |
State Reference | NC |
Altitude | msl single value : 23000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zdc.artcc |
Operator | common carrier : air carrier |
Make Model Name | HS 125 Series 1-600 |
Operating Under FAR Part | Part 121 |
Flight Phase | descent : vacating altitude descent : intermediate altitude |
Route In Use | arrival : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : multi engine pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 5700 flight time type : 290 |
ASRS Report | 457067 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : multi engine pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical altitude deviation : excursion from assigned altitude other anomaly other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : master caution light other flight crewa other flight crewb |
Resolutory Action | controller : provided flight assist controller : issued new clearance flight crew : regained aircraft control flight crew : overrode automation flight crew : exited adverse environment |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
During descent into rdu, nose down trim was applied with trim switch (autoplt and autothrottle off) and trim runway to full nose down. The only way to stop the trim was to turn the autoplt master switch off. Field was IFR and with autoplt master off the mode control panel was lost and no navigation signals received. Once aircraft back under control autoplt master turned back on resulting in excessive right ruder (yaw damper) and the trim running full forward. Autoplt master turned back on manual trim available and restored the mode control panel. Hand flown approach flown into rdu. Digital flight guidance computer downloaded 17 errors appeared all from takeoff when a squat switch was faulty, requiring the override switch to be used to bring the gear up. No errors were detected during descent by dfgc (digital flight guidance). The DFDR (digital flight data recorder) was downloaded, but have not heard results yet.
Original NASA ASRS Text
Title: MLG DSCNT TO RDU EXPERIENCES RUN AWAY STABILIZER TRIM AS THE FIRST OF SEVERAL ACFT EQUIP MALFUNCTIONS PRIOR TO LNDG.
Narrative: DURING DSCNT INTO RDU, NOSE DOWN TRIM WAS APPLIED WITH TRIM SWITCH (AUTOPLT AND AUTOTHROTTLE OFF) AND TRIM RWY TO FULL NOSE DOWN. THE ONLY WAY TO STOP THE TRIM WAS TO TURN THE AUTOPLT MASTER SWITCH OFF. FIELD WAS IFR AND WITH AUTOPLT MASTER OFF THE MODE CTL PANEL WAS LOST AND NO NAV SIGNALS RECEIVED. ONCE ACFT BACK UNDER CTL AUTOPLT MASTER TURNED BACK ON RESULTING IN EXCESSIVE R RUDER (YAW DAMPER) AND THE TRIM RUNNING FULL FORWARD. AUTOPLT MASTER TURNED BACK ON MANUAL TRIM AVAILABLE AND RESTORED THE MODE CTL PANEL. HAND FLOWN APCH FLOWN INTO RDU. DIGITAL FLT GUIDANCE COMPUTER DOWNLOADED 17 ERRORS APPEARED ALL FROM TKOF WHEN A SQUAT SWITCH WAS FAULTY, REQUIRING THE OVERRIDE SWITCH TO BE USED TO BRING THE GEAR UP. NO ERRORS WERE DETECTED DURING DSCNT BY DFGC (DIGITAL FLT GUIDANCE). THE DFDR (DIGITAL FLT DATA RECORDER) WAS DOWNLOADED, BUT HAVE NOT HEARD RESULTS YET.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.