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|
Attributes | |
ACN | 463102 |
Time | |
Date | 200002 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : ojc.airport |
State Reference | KS |
Environment | |
Flight Conditions | VMC |
Aircraft 1 | |
Controlling Facilities | tower : ojc.tower tower : ord.tower |
Operator | general aviation : personal |
Make Model Name | Bonanza 36 |
Operating Under FAR Part | Part 91 |
Flight Phase | descent : approach |
Route In Use | approach : traffic pattern approach : visual |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | instruction : instructor oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : cfi pilot : multi engine |
Experience | flight time last 90 days : 125 flight time total : 2130 flight time type : 11 |
ASRS Report | 463102 |
Person 2 | |
Affiliation | other |
Function | instruction : trainee |
Qualification | pilot : commercial pilot : instrument pilot : multi engine |
Experience | flight time last 90 days : 20 flight time total : 1850 flight time type : 800 |
ASRS Report | 463022 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : engine other flight crewa other flight crewb |
Resolutory Action | flight crew : declared emergency flight crew : landed in emergency condition |
Consequence | faa : investigated other other |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Aircraft |
Narrative:
A similar form has been submitted by the pilot describing this event. As the pilot was executing a simulated emergency approach and landing at the ojc airport, it became apparent the aircraft would not reach the runway without applying additional power. As the pilot applied full power, the engine coughed and never produced additional power. Being at low altitude and insufficient power, the aircraft descended, contacted the ground in level altitude, but resulted in a collapsed nose gear. No injuries were sustained. The engine was a 20 hour factory remanufactured engine installed during the preceding 90 days.
Original NASA ASRS Text
Title: WHEN PLT OF A BEECH A36 ATTEMPTED TO ADD FULL PWR DURING A SIMULATED FORCED LNDG TRAINING FLT, THE ENG DID NOT RESPOND, CAUSING A FORCED LNDG JUST SHORT OF THE RWY. THE NOSE GEAR WAS DAMAGED.
Narrative: A SIMILAR FORM HAS BEEN SUBMITTED BY THE PLT DESCRIBING THIS EVENT. AS THE PLT WAS EXECUTING A SIMULATED EMER APCH AND LNDG AT THE OJC ARPT, IT BECAME APPARENT THE ACFT WOULD NOT REACH THE RWY WITHOUT APPLYING ADDITIONAL PWR. AS THE PLT APPLIED FULL PWR, THE ENG COUGHED AND NEVER PRODUCED ADDITIONAL PWR. BEING AT LOW ALT AND INSUFFICIENT PWR, THE ACFT DSNDED, CONTACTED THE GND IN LEVEL ALT, BUT RESULTED IN A COLLAPSED NOSE GEAR. NO INJURIES WERE SUSTAINED. THE ENG WAS A 20 HR FACTORY REMANUFACTURED ENG INSTALLED DURING THE PRECEDING 90 DAYS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.