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|
Attributes | |
ACN | 483487 |
Time | |
Date | 200008 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Altitude | agl single value : 100 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : d10.tracon |
Operator | common carrier : air carrier |
Make Model Name | MD-82 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : commercial pilot : instrument pilot : multi engine pilot : atp |
Experience | flight time last 90 days : 171 flight time total : 14640 flight time type : 225 |
ASRS Report | 483487 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : nose gear position indication other flight crewa other flight crewb |
Resolutory Action | flight crew : landed as precaution |
Consequence | other other |
Supplementary | |
Problem Areas | Maintenance Human Performance Flight Crew Human Performance Environmental Factor Aircraft Company |
Primary Problem | Aircraft |
Narrative:
After takeoff the nose landing gear would not fully retract. The captain elected not to cycle the gear because of slipstream noise and a temporary burning rubber odor. We had the gear examined by air rescue fire fighting (arff) during a low pass. It appeared to them that the right nose tire was shredded. Arff looked closely at the gear after landing and could see no damage so we taxied to the gate with their escort. Company maintenance found the strut was deflated without apparent fluid leakage. The preflight strut extension wasn't very high, but seemed to be within operating manual limits. I thought the strut was under a load.
Original NASA ASRS Text
Title: AN MD82, IMMEDIATELY AFTER TKOF, RETURNED TO THE FIELD DUE TO UNABLE TO RETRACT THE NOSE LNDG GEAR CAUSED BY A DEFLATED STRUT.
Narrative: AFTER TKOF THE NOSE LNDG GEAR WOULD NOT FULLY RETRACT. THE CAPT ELECTED NOT TO CYCLE THE GEAR BECAUSE OF SLIPSTREAM NOISE AND A TEMPORARY BURNING RUBBER ODOR. WE HAD THE GEAR EXAMINED BY AIR RESCUE FIRE FIGHTING (ARFF) DURING A LOW PASS. IT APPEARED TO THEM THAT THE R NOSE TIRE WAS SHREDDED. ARFF LOOKED CLOSELY AT THE GEAR AFTER LNDG AND COULD SEE NO DAMAGE SO WE TAXIED TO THE GATE WITH THEIR ESCORT. COMPANY MAINT FOUND THE STRUT WAS DEFLATED WITHOUT APPARENT FLUID LEAKAGE. THE PREFLT STRUT EXTENSION WASN'T VERY HIGH, BUT SEEMED TO BE WITHIN OPERATING MANUAL LIMITS. I THOUGHT THE STRUT WAS UNDER A LOAD.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.