37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 485913 |
Time | |
Date | 200009 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dtw.airport |
State Reference | MI |
Altitude | agl single value : 100 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : dtw.tower |
Operator | common carrier : air carrier |
Make Model Name | DC-9 30 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other vortac |
Flight Phase | climbout : takeoff |
Route In Use | departure sid : 21l |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : cfi pilot : flight engineer pilot : instrument pilot : multi engine pilot : commercial |
Experience | flight time last 90 days : 200 flight time total : 15000 flight time type : 3000 |
ASRS Report | 485913 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : multi engine |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : #1 engine indications other flight crewa other flight crewb |
Resolutory Action | controller : issued new clearance flight crew : declared emergency |
Consequence | other other other |
Supplementary | |
Problem Areas | Aircraft Environmental Factor |
Primary Problem | Aircraft |
Narrative:
After lift-off at 100 ft AGL left engine lost 80% power with subsequent vibration. Engine was shut down after clean-up and engine failure checklist was accomplished. Declared an emergency, briefed flight attendants and passenger and performed a normal engine-out landing. After touchdown and taxi-in left hydraulic system fluid quantity went to zero. Selected right brake system and requested a tow-in to the gate. Postflt inspection revealed turbine section damage (extensive) and vibration appeared to have loosened hydraulic line for left thrust reverser. Ground shift allowed hydraulic pressure to thrust reverser through thrust reverser isolation valve resulting in loss of fluid after touchdown.
Original NASA ASRS Text
Title: A DC9-30 ON LIFTOFF AT 100 FT AGL DECLARED AN EMER AND DIVERTED DUE TO #1 ENG LOSS OF PWR CAUSED BY TURBINE BLADE FAILURE.
Narrative: AFTER LIFT-OFF AT 100 FT AGL L ENG LOST 80% PWR WITH SUBSEQUENT VIBRATION. ENG WAS SHUT DOWN AFTER CLEAN-UP AND ENG FAILURE CHKLIST WAS ACCOMPLISHED. DECLARED AN EMER, BRIEFED FLT ATTENDANTS AND PAX AND PERFORMED A NORMAL ENG-OUT LNDG. AFTER TOUCHDOWN AND TAXI-IN L HYD SYS FLUID QUANTITY WENT TO ZERO. SELECTED R BRAKE SYS AND REQUESTED A TOW-IN TO THE GATE. POSTFLT INSPECTION REVEALED TURBINE SECTION DAMAGE (EXTENSIVE) AND VIBRATION APPEARED TO HAVE LOOSENED HYD LINE FOR L THRUST REVERSER. GND SHIFT ALLOWED HYD PRESSURE TO THRUST REVERSER THROUGH THRUST REVERSER ISOLATION VALVE RESULTING IN LOSS OF FLUID AFTER TOUCHDOWN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.