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|
Attributes | |
ACN | 495428 |
Time | |
Date | 200012 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : crp.airport |
State Reference | TX |
Altitude | msl single value : 2000 |
Environment | |
Flight Conditions | Mixed |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : crp.tracon |
Operator | common carrier : air carrier |
Make Model Name | DC-9 50 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other vortac |
Flight Phase | climbout : takeoff |
Route In Use | departure : other published ifr departure |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 8000 flight time type : 2000 |
ASRS Report | 495428 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : #2 engine indicator other flight crewa other flight crewb other other : person 3 |
Resolutory Action | flight crew : diverted to another airport flight crew : declared emergency |
Consequence | other other |
Supplementary | |
Problem Areas | Maintenance Human Performance Aircraft Airport Environmental Factor |
Primary Problem | Aircraft |
Narrative:
On takeoff roll at crp, 10 KTS prior to V1, aircraft experienced 3 loud bangs. No loss in engine power was observed. Aircraft departed and lifted off in what might have been some loss in power. Aircraft was 'cleaned up' and power reduced. All system instrument appeared normal, however, engines sounded very loud, a 'whiney' sound. Flight attendants confirmed engine noise and believed we blew out tires on our takeoff roll. Additionally, the forward cargo door light was on. A cockpit jump seat rider who was in the passenger cabin was brought onto the flight deck to assist. He was not sure if we had engine and/or tire problems. An emergency was declared and began vectors for an ILS back to crp. We were not sure if we had had 1) cargo which effected the engines, 2) blown ties which FOD'ed the engines, or 3) straight ene problems. We ordered a runway inspection for contamination check. Aircraft was pressurizing which eliminated the cargo light problem. On final approach, runway was still being inspected. A go around was performed and engine's compressor stalled about 3 times. Power was reduced and engines stabilized. There was no debris found on runway and another approach and landing was performed. The #2 engine sustained significant fan blade damage necessitating an engine change. No injuries reported. Only damage was to #2 engine. Callback conversation with reporter revealed the following information: the reporter stated the fan blades were extensively damaged and required an engine change. The reporter said it appeared to be FOD, but maintenance has not advised their findings.
Original NASA ASRS Text
Title: A DC9-50 ON TKOF CLB DECLARED AN EMER AND DIVERTED DUE TO #2 ENG STALLING AND LOSS OF PWR.
Narrative: ON TKOF ROLL AT CRP, 10 KTS PRIOR TO V1, ACFT EXPERIENCED 3 LOUD BANGS. NO LOSS IN ENG PWR WAS OBSERVED. ACFT DEPARTED AND LIFTED OFF IN WHAT MIGHT HAVE BEEN SOME LOSS IN PWR. ACFT WAS 'CLEANED UP' AND PWR REDUCED. ALL SYS INST APPEARED NORMAL, HOWEVER, ENGS SOUNDED VERY LOUD, A 'WHINEY' SOUND. FLT ATTENDANTS CONFIRMED ENG NOISE AND BELIEVED WE BLEW OUT TIRES ON OUR TKOF ROLL. ADDITIONALLY, THE FORWARD CARGO DOOR LIGHT WAS ON. A COCKPIT JUMP SEAT RIDER WHO WAS IN THE PAX CABIN WAS BROUGHT ONTO THE FLT DECK TO ASSIST. HE WAS NOT SURE IF WE HAD ENG AND/OR TIRE PROBS. AN EMER WAS DECLARED AND BEGAN VECTORS FOR AN ILS BACK TO CRP. WE WERE NOT SURE IF WE HAD HAD 1) CARGO WHICH EFFECTED THE ENGS, 2) BLOWN TIES WHICH FOD'ED THE ENGS, OR 3) STRAIGHT ENE PROBS. WE ORDERED A RWY INSPECTION FOR CONTAMINATION CHK. ACFT WAS PRESSURIZING WHICH ELIMINATED THE CARGO LIGHT PROB. ON FINAL APCH, RWY WAS STILL BEING INSPECTED. A GAR WAS PERFORMED AND ENG'S COMPRESSOR STALLED ABOUT 3 TIMES. PWR WAS REDUCED AND ENGS STABILIZED. THERE WAS NO DEBRIS FOUND ON RWY AND ANOTHER APCH AND LNDG WAS PERFORMED. THE #2 ENG SUSTAINED SIGNIFICANT FAN BLADE DAMAGE NECESSITATING AN ENG CHANGE. NO INJURIES RPTED. ONLY DAMAGE WAS TO #2 ENG. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE FAN BLADES WERE EXTENSIVELY DAMAGED AND REQUIRED AN ENG CHANGE. THE RPTR SAID IT APPEARED TO BE FOD, BUT MAINT HAS NOT ADVISED THEIR FINDINGS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.