Narrative:

During pre-dock runup for a 'B' check, mechanics found the pneumatic flex hose from the main duct to the #1 engine start valve ruptured. After consulting company personnel and engineering, it was decided that the start valve could be manually opened. Engineering authority/authorized document was issued for removing and capping the ruptured line as well as placing the engine start valve on MEL. On climb and from ZZZ, the #1 engine pneumatic pressure pegged out on the pneumatic pressure gauge. A #1 bleed trip was experienced by the flight crew. The flight continued to mco at FL250. This situation arose due to a couple of items: 1) due to a failure on the mechanic's part to notice a tee-fitting downstream of the pressure regulator for the slat valve that is plumbed to the bleed valve regulator. 2) the vagueness of the idc in this area contributed to the tee-fitting being missed upon first inspection. 3) the part we needed wasn't in stock in ZZZ and would not arrive for 4 or 5 hours, so I put pressure on myself unknowingly to dispatch the airplane.

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Original NASA ASRS Text

Title: A B737-200 WAS DISPATCHED IN NON COMPLIANCE WITH THE L ENG START VALVE DEFERRED AS INOP ELECTRICALLY BUT MEL SPECIAL PROCS WERE NOT ACCOMPLISHED.

Narrative: DURING PRE-DOCK RUNUP FOR A 'B' CHK, MECHS FOUND THE PNEUMATIC FLEX HOSE FROM THE MAIN DUCT TO THE #1 ENG START VALVE RUPTURED. AFTER CONSULTING COMPANY PERSONNEL AND ENGINEERING, IT WAS DECIDED THAT THE START VALVE COULD BE MANUALLY OPENED. ENGINEERING AUTH DOCUMENT WAS ISSUED FOR REMOVING AND CAPPING THE RUPTURED LINE AS WELL AS PLACING THE ENG START VALVE ON MEL. ON CLB AND FROM ZZZ, THE #1 ENG PNEUMATIC PRESSURE PEGGED OUT ON THE PNEUMATIC PRESSURE GAUGE. A #1 BLEED TRIP WAS EXPERIENCED BY THE FLC. THE FLT CONTINUED TO MCO AT FL250. THIS SIT AROSE DUE TO A COUPLE OF ITEMS: 1) DUE TO A FAILURE ON THE MECH'S PART TO NOTICE A TEE-FITTING DOWNSTREAM OF THE PRESSURE REGULATOR FOR THE SLAT VALVE THAT IS PLUMBED TO THE BLEED VALVE REGULATOR. 2) THE VAGUENESS OF THE IDC IN THIS AREA CONTRIBUTED TO THE TEE-FITTING BEING MISSED UPON FIRST INSPECTION. 3) THE PART WE NEEDED WASN'T IN STOCK IN ZZZ AND WOULD NOT ARRIVE FOR 4 OR 5 HRS, SO I PUT PRESSURE ON MYSELF UNKNOWINGLY TO DISPATCH THE AIRPLANE.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.