Narrative:

The aircraft was terminated for the evening and the captain had already left. The flight attendants notified me that there was a broken trash receptacle hinge/door in the aft lavatory. I advised the operations agent who told me that a mechanic was notified and on his way over to the airplane. I then made a logbook write-up of the discrepancy, and asked the operations agent to pass this fact along to the mechanic as well. I neglected to coordinate with dispatch or with duty control on this matter. I remember being told at some point in my past that this is necessary, but that night I did not think to do it. The next day I learned that the aircraft was operated unknowingly with the write-up still open. In the future, I will notify duty control -- always.

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Original NASA ASRS Text

Title: A B737 WAS DISPATCHED IN NON COMPLIANCE WITH AN OPEN AND UNANSWERED LOG RPT.

Narrative: THE ACFT WAS TERMINATED FOR THE EVENING AND THE CAPT HAD ALREADY LEFT. THE FLT ATTENDANTS NOTIFIED ME THAT THERE WAS A BROKEN TRASH RECEPTACLE HINGE/DOOR IN THE AFT LAVATORY. I ADVISED THE OPS AGENT WHO TOLD ME THAT A MECH WAS NOTIFIED AND ON HIS WAY OVER TO THE AIRPLANE. I THEN MADE A LOGBOOK WRITE-UP OF THE DISCREPANCY, AND ASKED THE OPS AGENT TO PASS THIS FACT ALONG TO THE MECH AS WELL. I NEGLECTED TO COORDINATE WITH DISPATCH OR WITH DUTY CTL ON THIS MATTER. I REMEMBER BEING TOLD AT SOME POINT IN MY PAST THAT THIS IS NECESSARY, BUT THAT NIGHT I DID NOT THINK TO DO IT. THE NEXT DAY I LEARNED THAT THE ACFT WAS OPERATED UNKNOWINGLY WITH THE WRITE-UP STILL OPEN. IN THE FUTURE, I WILL NOTIFY DUTY CTL -- ALWAYS.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.