Narrative:

Aircraft received a thorough preflight and pretkof checklist. Takeoff initiated on runway 10 at genesee county airport. At 200 ft AGL and 800 ft from departure end of runway 10, the engine failed. It acted as if someone had closed the throttle to idle. The boundary fence and other obstacles were approaching. I elected to close the throttle to avoid the possibility of a power surge. I made a full flap landing on the grass with no damage to the aircraft or objects on ground. I was not hurt. It was a normal grass field landing. The pre takeoff magneto check was totally normal and the engine had been operating normally on previous flts up until failure. Engine ran fine after restart on ground. Subsequent review by an a&P and ia found all fuel and aircraft system normal. Reason for the engine failure was 'butter nuts' in the carburetor air box. Apparently an animal had stored them in the scat tubing and air box for the carburetor heat system. Once the 'butter nuts' were removed, the aircraft was inspected, test flown and returned to service by the a&P and ia. Subsequent operations have been totally normal.

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Original NASA ASRS Text

Title: C172 PLT HAD ENG FAILURE AND FORCED LNDG ON TKOF.

Narrative: ACFT RECEIVED A THOROUGH PREFLT AND PRETKOF CHKLIST. TKOF INITIATED ON RWY 10 AT GENESEE COUNTY ARPT. AT 200 FT AGL AND 800 FT FROM DEP END OF RWY 10, THE ENG FAILED. IT ACTED AS IF SOMEONE HAD CLOSED THE THROTTLE TO IDLE. THE BOUNDARY FENCE AND OTHER OBSTACLES WERE APCHING. I ELECTED TO CLOSE THE THROTTLE TO AVOID THE POSSIBILITY OF A PWR SURGE. I MADE A FULL FLAP LNDG ON THE GRASS WITH NO DAMAGE TO THE ACFT OR OBJECTS ON GND. I WAS NOT HURT. IT WAS A NORMAL GRASS FIELD LNDG. THE PRE TKOF MAGNETO CHK WAS TOTALLY NORMAL AND THE ENG HAD BEEN OPERATING NORMALLY ON PREVIOUS FLTS UP UNTIL FAILURE. ENG RAN FINE AFTER RESTART ON GND. SUBSEQUENT REVIEW BY AN A&P AND IA FOUND ALL FUEL AND ACFT SYS NORMAL. REASON FOR THE ENG FAILURE WAS 'BUTTER NUTS' IN THE CARB AIR BOX. APPARENTLY AN ANIMAL HAD STORED THEM IN THE SCAT TUBING AND AIR BOX FOR THE CARB HEAT SYS. ONCE THE 'BUTTER NUTS' WERE REMOVED, THE ACFT WAS INSPECTED, TEST FLOWN AND RETURNED TO SVC BY THE A&P AND IA. SUBSEQUENT OPS HAVE BEEN TOTALLY NORMAL.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.