Narrative:

High speed abort due to severe vibration. At about 100 KTS the aircraft began shaking severely. Captain aborted takeoff. Lost nosewheel steering. After clearing runway maintenance came and told us the nose gear scissors link had become disconnected. Vibration caused damage inside aircraft to ceiling panels, luggage racks, equipment racks and door 3R came open. Flight control checks were normal before takeoff, scissors pin probably came loose on takeoff roll.

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Original NASA ASRS Text

Title: A DC10 CREW EXECUTED A REJECTED TKOF AT DTW, WHEN ENCOUNTERING A SEVERE VIBRATION ON TKOF ROLL.

Narrative: HIGH SPD ABORT DUE TO SEVERE VIBRATION. AT ABOUT 100 KTS THE ACFT BEGAN SHAKING SEVERELY. CAPT ABORTED TKOF. LOST NOSEWHEEL STEERING. AFTER CLRING RWY MAINT CAME AND TOLD US THE NOSE GEAR SCISSORS LINK HAD BECOME DISCONNECTED. VIBRATION CAUSED DAMAGE INSIDE ACFT TO CEILING PANELS, LUGGAGE RACKS, EQUIP RACKS AND DOOR 3R CAME OPEN. FLT CTL CHKS WERE NORMAL BEFORE TKOF, SCISSORS PIN PROBABLY CAME LOOSE ON TKOF ROLL.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.