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|
Attributes | |
ACN | 524460 |
Time | |
Date | 200109 |
Day | Mon |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | airport : bos.airport |
State Reference | MA |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : rfd.tower |
Operator | common carrier : air carrier |
Make Model Name | B757 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : multi engine |
Experience | flight time last 90 days : 120 flight time total : 15000 flight time type : 450 |
ASRS Report | 524460 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical inflight encounter : birds other anomaly other |
Independent Detector | other flight crewa other flight crewb other other : pax 4 |
Resolutory Action | controller : provided flight assist flight crew : landed in emergency condition flight crew : declared emergency other |
Consequence | faa : reviewed incident with flight crew other other other |
Supplementary | |
Problem Areas | ATC Human Performance Airport Environmental Factor Aircraft |
Primary Problem | Airport |
Narrative:
On takeoff from bos runway 22R, at rotation felt yaw to left. Thought we had hit something, blown tire, or had compressor stall on #1. Stayed in area to assess problem. Flight attendant reported passenger reported smoke and fire from left side. Precautionary shutdown of #1 engine. Never raised gear because of possibility that problem was that we hit something. Low pass over runway for ger inspection. Checked ok. Landed ok. Subsequent investigation revealed bird to #1 engine.
Original NASA ASRS Text
Title: A B757 PIC PERFORMS A TWR FLY-BY FOR GEAR INSPECTION AFTER AN INFLT ENG SHUT DOWN CREATED BY A BIRD STRIKE AT BOS, MA.
Narrative: ON TKOF FROM BOS RWY 22R, AT ROTATION FELT YAW TO LEFT. THOUGHT WE HAD HIT SOMETHING, BLOWN TIRE, OR HAD COMPRESSOR STALL ON #1. STAYED IN AREA TO ASSESS PROBLEM. FLT ATTENDANT REPORTED PAX REPORTED SMOKE AND FIRE FROM LEFT SIDE. PRECAUTIONARY SHUTDOWN OF #1 ENGINE. NEVER RAISED GEAR BECAUSE OF POSSIBILITY THAT PROBLEM WAS THAT WE HIT SOMETHING. LOW PASS OVER RWY FOR GER INSPECTION. CHECKED OK. LANDED OK. SUBSEQUENT INVESTIGATION REVEALED BIRD TO #1 ENG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.