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|
Attributes | |
ACN | 524810 |
Time | |
Date | 200109 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B727-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : taxi ground : maintenance |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | maintenance : technician |
Qualification | technician : airframe technician : powerplant |
Experience | maintenance technician : 13 |
ASRS Report | 524810 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper documentation maintenance problem : improper maintenance non adherence : published procedure non adherence : far non adherence : company policies other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact other |
Factors | |
Maintenance | contributing factor : schedule pressure performance deficiency : training performance deficiency : testing performance deficiency : repair performance deficiency : non compliance with legal requirements performance deficiency : inspection performance deficiency : fault isolation performance deficiency : logbook entry |
Supplementary | |
Problem Areas | Aircraft Maintenance Human Performance Company |
Primary Problem | Maintenance Human Performance |
Narrative:
After 'light off' of #1 engine, on push back, the captain informed me that #1 tank aft boost pump circuit breaker had popped, resulting in a gate return (since they are prohibited from resetting boost pump or fuel qty, circuit breaker's) I noted (as captain did) that it happened as the engine generator took over from APU generator. I was confident this popped circuit breaker resulted from a power surge, which later, my suspicions proved right. I reset the circuit breaker, operations checked pump several times/mins with no further faults. It should be noted we also had another problem with the aircraft. The pneumatic duct supply gauge on the second officers panel was inoperative, again. It acted up earlier. In short ' the plane didn't want to leave,' and I knew it was a generation charge fluctuation that caused the circuit breaker to pop.
Original NASA ASRS Text
Title: B727-200 CREW HAD ELECTRICAL PROB THAT REQUIRED RETURN TO THE GATE.
Narrative: AFTER 'LIGHT OFF' OF #1 ENG, ON PUSH BACK, THE CAPT INFORMED ME THAT #1 TANK AFT BOOST PUMP CB HAD POPPED, RESULTING IN A GATE RETURN (SINCE THEY ARE PROHIBITED FROM RESETTING BOOST PUMP OR FUEL QTY, CB'S) I NOTED (AS CAPT DID) THAT IT HAPPENED AS THE ENG GENERATOR TOOK OVER FROM APU GENERATOR. I WAS CONFIDENT THIS POPPED CB RESULTED FROM A PWR SURGE, WHICH LATER, MY SUSPICIONS PROVED RIGHT. I RESET THE CB, OPS CHECKED PUMP SEVERAL TIMES/MINS WITH NO FURTHER FAULTS. IT SHOULD BE NOTED WE ALSO HAD ANOTHER PROB WITH THE ACFT. THE PNEUMATIC DUCT SUPPLY GAUGE ON THE SECOND OFFICERS PANEL WAS INOP, AGAIN. IT ACTED UP EARLIER. IN SHORT ' THE PLANE DIDN'T WANT TO LEAVE,' AND I KNEW IT WAS A GENERATION CHARGE FLUCTUATION THAT CAUSED THE CB TO POP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.