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|
Attributes | |
ACN | 542822 |
Time | |
Date | 200203 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : lga.tower |
Operator | common carrier : air carrier |
Make Model Name | A310 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | ground : maintenance |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | maintenance : technician |
Qualification | technician : airframe technician : powerplant |
ASRS Report | 542822 |
Person 2 | |
Affiliation | company : air carrier |
Function | maintenance : technician |
Qualification | technician : powerplant technician : airframe |
ASRS Report | 542823 |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance non adherence : far non adherence : published procedure |
Independent Detector | aircraft equipment other aircraft equipment : engine press quantity indications other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport |
Consequence | other other |
Factors | |
Maintenance | performance deficiency : installation performance deficiency : testing performance deficiency : inspection |
Supplementary | |
Problem Areas | Maintenance Human Performance Aircraft Environmental Factor |
Primary Problem | Maintenance Human Performance |
Narrative:
Low pressure turbine cooling of manifold and oil lines were disconnected by another mechanic on 03/fri/02. I installed a low pressure turbine manifold and oil line on 03/xx/02 and wet motored on 03/mon/02 and found no leaks. Crew chief log on run-up noted oil leak. Checked engine over and found no evidence of oil or leaks on 03/thu/02. No discrepancy on leaking oil. Checked oil quantity and found to be good. Aircraft was dispatched to air carrier loading area at XA35 03/sat/02. No oil leaks found. Air interrupt on 03/sat/02 at approximately XA50.
Original NASA ASRS Text
Title: AN AIRBUS 310 SHORTLY AFTER TKOF RETURNED TO THE FIELD DUE TO LOSS OF OIL PRESSURE AND QUANTITY FROM LEAKING OIL SCAVENGE LINE.
Narrative: LOW PRESSURE TURBINE COOLING OF MANIFOLD AND OIL LINES WERE DISCONNECTED BY ANOTHER MECH ON 03/FRI/02. I INSTALLED A LOW PRESSURE TURBINE MANIFOLD AND OIL LINE ON 03/XX/02 AND WET MOTORED ON 03/MON/02 AND FOUND NO LEAKS. CREW CHIEF LOG ON RUN-UP NOTED OIL LEAK. CHKED ENG OVER AND FOUND NO EVIDENCE OF OIL OR LEAKS ON 03/THU/02. NO DISCREPANCY ON LEAKING OIL. CHKED OIL QUANTITY AND FOUND TO BE GOOD. ACFT WAS DISPATCHED TO ACR LOADING AREA AT XA35 03/SAT/02. NO OIL LEAKS FOUND. AIR INTERRUPT ON 03/SAT/02 AT APPROX XA50.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.