37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 565852 |
Time | |
Date | 200211 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Environment | |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : d10.tracon |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : initial climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
ASRS Report | 565852 |
Person 2 | |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance non adherence : company policies other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | controller : issued new clearance flight crew : diverted to another airport flight crew : landed as precaution other |
Consequence | other other |
Factors | |
Maintenance | contributing factor : schedule pressure performance deficiency : non compliance with legal requirements performance deficiency : repair performance deficiency : testing performance deficiency : fault isolation |
Supplementary | |
Problem Areas | Aircraft Company Maintenance Human Performance |
Primary Problem | Aircraft |
Narrative:
After takeoff on runway 36R, it became immediately apparent that the aircraft was not pressurizing properly. The outflow valve was still open. At about 1000 ft, an attempt to operate the pressurization system in manual was ineffective. We leveled at 5000 ft and took vectors and returned to dfw. The aircraft had a similar pressurization problem previously. Included in the write-up was a needed inspection for a very soft overweight landing.
Original NASA ASRS Text
Title: MD80 CREW WAS UNABLE TO PRESSURIZE THE ACFT. THIS PROB WAS A REPEAT OF PREVIOUS DISCREPANCY.
Narrative: AFTER TKOF ON RWY 36R, IT BECAME IMMEDIATELY APPARENT THAT THE ACFT WAS NOT PRESSURIZING PROPERLY. THE OUTFLOW VALVE WAS STILL OPEN. AT ABOUT 1000 FT, AN ATTEMPT TO OPERATE THE PRESSURIZATION SYS IN MANUAL WAS INEFFECTIVE. WE LEVELED AT 5000 FT AND TOOK VECTORS AND RETURNED TO DFW. THE ACFT HAD A SIMILAR PRESSURIZATION PROB PREVIOUSLY. INCLUDED IN THE WRITE-UP WAS A NEEDED INSPECTION FOR A VERY SOFT OVERWT LNDG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.