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|
Attributes | |
ACN | 613976 |
Time | |
Date | 200403 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : ict.airport |
State Reference | KS |
Altitude | msl single value : 37000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zkc.artcc tower : lax.tower |
Operator | general aviation : corporate |
Make Model Name | Learjet 35 |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : corporate |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp |
Experience | flight time last 90 days : 75 flight time total : 2600 flight time type : 75 |
ASRS Report | 613976 |
Person 2 | |
Affiliation | company : corporate |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly |
Independent Detector | other flight crewa other flight crewb other other : 3 |
Resolutory Action | aircraft : evacuated controller : provided flight assist controller : issued new clearance flight crew : landed in emergency condition flight crew : declared emergency flight crew : diverted to another airport other |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Passenger noted us to an abnormal smell. We started a precautionary descent, during descent smoke started entering cockpit. We declared an emergency. ATC vectored us to wichita, ks, where we landed and evacuate/evacuationed the aircraft safely. Callback conversation with reporter revealed the following information: the reporter told of a burned up recirculating fan. The fan impeller blades are made of plastic and they jammed forcing the motor to stop turning. As a result, the electrical motor began smoking. After the motor was replaced, no further problems were evident.
Original NASA ASRS Text
Title: LJ35 CREW HAD THE PAX TELL THEM OF AN ABNORMAL SMELL IN THE CABIN. DURING DSCNT, SMOKE STARTED ENTERING THE COCKPIT.
Narrative: PAX NOTED US TO AN ABNORMAL SMELL. WE STARTED A PRECAUTIONARY DSCNT, DURING DSCNT SMOKE STARTED ENTERING COCKPIT. WE DECLARED AN EMER. ATC VECTORED US TO WICHITA, KS, WHERE WE LANDED AND EVACED THE ACFT SAFELY. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR TOLD OF A BURNED UP RECIRCULATING FAN. THE FAN IMPELLER BLADES ARE MADE OF PLASTIC AND THEY JAMMED FORCING THE MOTOR TO STOP TURNING. AS A RESULT, THE ELECTRICAL MOTOR BEGAN SMOKING. AFTER THE MOTOR WAS REPLACED, NO FURTHER PROBS WERE EVIDENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.