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Attributes | |
ACN | 653042 |
Time | |
Date | 200504 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Experience | flight time last 90 days : 200 flight time total : 8000 flight time type : 5000 |
ASRS Report | 653042 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Experience | flight time last 90 days : 220 flight time total : 12000 flight time type : 8100 |
ASRS Report | 653043 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : #2 engine indications other flight crewa other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft |
Primary Problem | Aircraft |
Narrative:
On start; #2 engine started normally; then rolled back and shut down. Subsequent start was successful. Taxi was normal. Just after brake release; #2 engine rolled back and operated erratically. Aborted takeoff at approximately 25 KTS. Returned to gate and gave airplane to maintenance. Supplemental information from acn 653043: at starter cut-out at 46% N2; the engine rolled back and fuel flow indicated zero. As I reached for the start lever; it became apparent that it was not all the way up and in the idle detent. We aborted the start at that time; motored the engine to ensure no fuel vapor accumulation and attempted another start. Callback conversation with reporter can 653042 revealed the following information: the story reporter got was the engine main fuel control was replaced. This is secondhand information from the technicians at the station where the event happened.
Original NASA ASRS Text
Title: AN MD80 ABORTED TKOF AT 25 KTS DUE TO #2 ENG ROLLBACK AND ERRATIC OP. CAUSED BY ENG MAIN FUEL CTL FAILURE.
Narrative: ON START; #2 ENG STARTED NORMALLY; THEN ROLLED BACK AND SHUT DOWN. SUBSEQUENT START WAS SUCCESSFUL. TAXI WAS NORMAL. JUST AFTER BRAKE RELEASE; #2 ENG ROLLED BACK AND OPERATED ERRATICALLY. ABORTED TKOF AT APPROX 25 KTS. RETURNED TO GATE AND GAVE AIRPLANE TO MAINT. SUPPLEMENTAL INFO FROM ACN 653043: AT STARTER CUT-OUT AT 46% N2; THE ENG ROLLED BACK AND FUEL FLOW INDICATED ZERO. AS I REACHED FOR THE START LEVER; IT BECAME APPARENT THAT IT WAS NOT ALL THE WAY UP AND IN THE IDLE DETENT. WE ABORTED THE START AT THAT TIME; MOTORED THE ENG TO ENSURE NO FUEL VAPOR ACCUMULATION AND ATTEMPTED ANOTHER START. CALLBACK CONVERSATION WITH RPTR CAN 653042 REVEALED THE FOLLOWING INFO: THE STORY RPTR GOT WAS THE ENG MAIN FUEL CTL WAS REPLACED. THIS IS SECONDHAND INFO FROM THE TECHNICIANS AT THE STATION WHERE THE EVENT HAPPENED.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.