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Attributes | |
ACN | 667670 |
Time | |
Date | 200508 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
ASRS Report | 667670 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other other other |
Supplementary | |
Problem Areas | Environmental Factor Weather Aircraft |
Primary Problem | Aircraft |
Narrative:
Just prior to V1; I heard a bang and the aircraft yawed to the right. I aborted the takeoff. After we came to a stop; we had the crash fire rescue equipment look over the aircraft. The brakes became hot and 1 tire deflated. All passenger were taken to the terminal via bus. Callback conversation with reporter revealed the following information: the reporter stated the airplane was removed from service and remained overnight. Maintenance made checks to the engines looking for anything that could cause a high power stall. Nothing was found and the airplane was returned to service where it operated normally.
Original NASA ASRS Text
Title: AN MD80 JUST PRIOR TO V1 CREW HEARD LOUD BANG AND ACFT YAWED TO R. TKOF ABORTED.
Narrative: JUST PRIOR TO V1; I HEARD A BANG AND THE ACFT YAWED TO THE R. I ABORTED THE TKOF. AFTER WE CAME TO A STOP; WE HAD THE CFR LOOK OVER THE ACFT. THE BRAKES BECAME HOT AND 1 TIRE DEFLATED. ALL PAX WERE TAKEN TO THE TERMINAL VIA BUS. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE AIRPLANE WAS REMOVED FROM SVC AND REMAINED OVERNIGHT. MAINT MADE CHKS TO THE ENGS LOOKING FOR ANYTHING THAT COULD CAUSE A HIGH PWR STALL. NOTHING WAS FOUND AND THE AIRPLANE WAS RETURNED TO SVC WHERE IT OPERATED NORMALLY.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.