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|
Attributes | |
ACN | 693695 |
Time | |
Date | 200604 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : zzz.artcc |
State Reference | US |
Altitude | msl single value : 30000 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zzz.artcc |
Operator | common carrier : air carrier |
Make Model Name | B767-300 and 300 ER |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
ASRS Report | 693695 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other other : 3 |
Resolutory Action | flight crew : diverted to another airport flight crew : overcame equipment problem |
Consequence | other other other |
Supplementary | |
Problem Areas | Environmental Factor Aircraft |
Primary Problem | Aircraft |
Narrative:
At FL300 flight attendants reported seeing red flashing light coming from overhead storage bin adjacent to seat xx. They also reported a loud swishing sound followed by what sounded like plugging a hole. There was some air noise remaining but somewhat subdued. After communication with maintenance control; I elected to divert to ZZZZ for repairs. Maintenance found the top rotating beacon shattered. Upon further investigation; they found the interior portion of the light loose above the overhead compartment and insulation up around the attachment hole where the light is normally mounted. We made an uneventful overweight landing at 278000 pounds and released the emergency equipment after we cleared the runway. Callback conversation with reporter revealed the following information: the reporter stated the glass was shattered and this lens glass is greater than .250 inch with no evidence of a bird strike. The reporter believed the diversion was warranted due to the unknown damage. Inspection by maintenance found the light lens shattered and the light assembly laying on the top surface of the overhead storage bin. The hole left by the light assembly had been filled with fuselage insulation. May have been previous damage or crack in the lens but not bird strike.
Original NASA ASRS Text
Title: A B767-300 ER ON CLB AT FL300 DIVERTED DUE TO CABIN ATTENDANTS RPTING RED FLASHING LIGHT AND SWISHING SOUND FROM CTR OVERHEAD STORAGE BIN.
Narrative: AT FL300 FLT ATTENDANTS RPTED SEEING RED FLASHING LIGHT COMING FROM OVERHEAD STORAGE BIN ADJACENT TO SEAT XX. THEY ALSO RPTED A LOUD SWISHING SOUND FOLLOWED BY WHAT SOUNDED LIKE PLUGGING A HOLE. THERE WAS SOME AIR NOISE REMAINING BUT SOMEWHAT SUBDUED. AFTER COM WITH MAINT CTL; I ELECTED TO DIVERT TO ZZZZ FOR REPAIRS. MAINT FOUND THE TOP ROTATING BEACON SHATTERED. UPON FURTHER INVESTIGATION; THEY FOUND THE INTERIOR PORTION OF THE LIGHT LOOSE ABOVE THE OVERHEAD COMPARTMENT AND INSULATION UP AROUND THE ATTACHMENT HOLE WHERE THE LIGHT IS NORMALLY MOUNTED. WE MADE AN UNEVENTFUL OVERWT LNDG AT 278000 LBS AND RELEASED THE EMER EQUIP AFTER WE CLRED THE RWY. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE GLASS WAS SHATTERED AND THIS LENS GLASS IS GREATER THAN .250 INCH WITH NO EVIDENCE OF A BIRD STRIKE. THE RPTR BELIEVED THE DIVERSION WAS WARRANTED DUE TO THE UNKNOWN DAMAGE. INSPECTION BY MAINT FOUND THE LIGHT LENS SHATTERED AND THE LIGHT ASSEMBLY LAYING ON THE TOP SURFACE OF THE OVERHEAD STORAGE BIN. THE HOLE LEFT BY THE LIGHT ASSEMBLY HAD BEEN FILLED WITH FUSELAGE INSULATION. MAY HAVE BEEN PREVIOUS DAMAGE OR CRACK IN THE LENS BUT NOT BIRD STRIKE.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.