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|
Attributes | |
ACN | 708154 |
Time | |
Date | 200608 |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Aircraft 1 | |
Controlling Facilities | tower : zzz.tower |
Operator | common carrier : air carrier |
Make Model Name | B737-700 |
Operating Under FAR Part | Part 121 |
Person 1 | |
Affiliation | company : air carrier |
Function | maintenance : lead technician |
ASRS Report | 708154 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance non adherence : far non adherence : published procedure |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other other |
Factors | |
Maintenance | contributing factor : schedule pressure performance deficiency : logbook entry performance deficiency : testing performance deficiency : non compliance with legal requirements |
Supplementary | |
Problem Areas | Maintenance Human Performance Environmental Factor Aircraft Chart Or Publication |
Primary Problem | Maintenance Human Performance |
Narrative:
Aircraft called in on a through flight reporting they had a bird strike. It was discovered there was a bird strike on the upper l-hand side of the radome. Some of the bird hit the base of the l-hand upper pitot probe. After a bird strike inspection; it was determined that no damage was done to the radome or the pitot probe. No evidence of the bird was in the probe. We disconnected the quick disconnect at the adm and blew low pressure nitrogen through the line to make sure there was no obstruction. The flight crew reported no inbound indication problems. The aircraft was released after no damage was found. No obstructions were found and no inbound indication problems. The aircraft had an aborted takeoff after a 20 KT split was observed. The pitot static test box was used and found no problems in the system. The pitot probe and adm were changed for precautionary reasons.
Original NASA ASRS Text
Title: A B737-700 HAD A BIRD STRIKE RPT THAT WAS CLRED BY INSPECTION AND A TEST OF THE UPPER L PITOT TUBE. SUBSEQUENT TKOF WAS ABORTED DUE TO 20 KT SPLIT BTWN SYS.
Narrative: ACFT CALLED IN ON A THROUGH FLT RPTING THEY HAD A BIRD STRIKE. IT WAS DISCOVERED THERE WAS A BIRD STRIKE ON THE UPPER L-HAND SIDE OF THE RADOME. SOME OF THE BIRD HIT THE BASE OF THE L-HAND UPPER PITOT PROBE. AFTER A BIRD STRIKE INSPECTION; IT WAS DETERMINED THAT NO DAMAGE WAS DONE TO THE RADOME OR THE PITOT PROBE. NO EVIDENCE OF THE BIRD WAS IN THE PROBE. WE DISCONNECTED THE QUICK DISCONNECT AT THE ADM AND BLEW LOW PRESSURE NITROGEN THROUGH THE LINE TO MAKE SURE THERE WAS NO OBSTRUCTION. THE FLT CREW RPTED NO INBOUND INDICATION PROBS. THE ACFT WAS RELEASED AFTER NO DAMAGE WAS FOUND. NO OBSTRUCTIONS WERE FOUND AND NO INBOUND INDICATION PROBS. THE ACFT HAD AN ABORTED TKOF AFTER A 20 KT SPLIT WAS OBSERVED. THE PITOT STATIC TEST BOX WAS USED AND FOUND NO PROBS IN THE SYS. THE PITOT PROBE AND ADM WERE CHANGED FOR PRECAUTIONARY REASONS.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.