37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 709197 |
Time | |
Date | 200609 |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : pdx.airport |
State Reference | OR |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-400 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : pushback |
Flight Plan | IFR |
Aircraft 2 | |
Controlling Facilities | tower : pdx.tower |
Operator | common carrier : air carrier |
Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : taxi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Experience | flight time last 90 days : 150 flight time type : 3500 |
ASRS Report | 709197 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | other anomaly other |
Independent Detector | other flight crewa other flight crewb other other : 3 |
Resolutory Action | flight crew : exited adverse environment |
Consequence | Other |
Supplementary | |
Problem Areas | Company ATC Human Performance Maintenance Human Performance Flight Crew Human Performance |
Primary Problem | Ambiguous |
Narrative:
Aircraft pushed off gate. Notified by push crew that aircraft YYY had an engine running at the gate we were being pushed past and the jetblast was interfering with their pushback. Tug driver chose to stop the push. Flight crew coordination with ground control to try to get aircraft YYY to shut down the engine so push could continue. Aircraft YYY advised they had no APU and started at the gate; after receiving approval from ground control. Flight crew could no longer communicate with the tug driver as his headset was being blown off. He finally held it on with both hands long enough for us to tell him to disconnect tug and leave the area. Our aircraft had been pushed about 1/2 way through a turn around to face outbound. Once crew was clear we taxied outbound without incident. Pushback crew was placed in a hazardous situation that fortunately ended without injury. Ground control acknowledged clearing aircraft YYY start at the gate; but did not tell our flight they had an engine running. Clearly notifying our flight crew would have allowed us to stop the push prior to getting the ground crew into jetblast.
Original NASA ASRS Text
Title: B737-400 FLT CREW DURING PUSHBACK HAS THE ACFT PLACED BEHIND ANOTHER ACFT WITH THE ENG RUNNING.
Narrative: ACFT PUSHED OFF GATE. NOTIFIED BY PUSH CREW THAT ACFT YYY HAD AN ENG RUNNING AT THE GATE WE WERE BEING PUSHED PAST AND THE JETBLAST WAS INTERFERING WITH THEIR PUSHBACK. TUG DRIVER CHOSE TO STOP THE PUSH. FLT CREW COORD WITH GND CTL TO TRY TO GET ACFT YYY TO SHUT DOWN THE ENG SO PUSH COULD CONTINUE. ACFT YYY ADVISED THEY HAD NO APU AND STARTED AT THE GATE; AFTER RECEIVING APPROVAL FROM GND CTL. FLT CREW COULD NO LONGER COMMUNICATE WITH THE TUG DRIVER AS HIS HEADSET WAS BEING BLOWN OFF. HE FINALLY HELD IT ON WITH BOTH HANDS LONG ENOUGH FOR US TO TELL HIM TO DISCONNECT TUG AND LEAVE THE AREA. OUR ACFT HAD BEEN PUSHED ABOUT 1/2 WAY THROUGH A TURN AROUND TO FACE OUTBOUND. ONCE CREW WAS CLR WE TAXIED OUTBOUND WITHOUT INCIDENT. PUSHBACK CREW WAS PLACED IN A HAZARDOUS SITUATION THAT FORTUNATELY ENDED WITHOUT INJURY. GND CTL ACKNOWLEDGED CLRING ACFT YYY START AT THE GATE; BUT DID NOT TELL OUR FLT THEY HAD AN ENG RUNNING. CLRLY NOTIFYING OUR FLT CREW WOULD HAVE ALLOWED US TO STOP THE PUSH PRIOR TO GETTING THE GND CREW INTO JETBLAST.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.