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|
Attributes | |
ACN | 728026 |
Time | |
Date | 200702 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : psp.airport |
State Reference | CA |
Altitude | agl single value : 340 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zla.artcc |
Operator | common carrier : air carrier |
Make Model Name | B757-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 728026 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | other |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Just prior to passing over psp we smelt a burnt odor coming from the captain's vent that appeared intermittently. We proceeded per the air conditioning smoke QRH. Coordination with phx and based on the situation and aircraft history the left pack was left shut down. No smoke was smelt after the left pack was shut down. The problem being isolated we returned to phx and went into holding to burn fuel down. During holding we also noticed in the left corner of the captain's fwd window that there had been some arcing and suspect that may have actually been a contributing cause.
Original NASA ASRS Text
Title: A B757-200 AT FL340 OVER PSP RETURNED TO THE DEP ARPT DUE TO BURNED ODOR FROM CAPT'S VENT. SHUT DOWN L PACK AND ODOR DISSIPATED.
Narrative: JUST PRIOR TO PASSING OVER PSP WE SMELT A BURNT ODOR COMING FROM THE CAPT'S VENT THAT APPEARED INTERMITTENTLY. WE PROCEEDED PER THE AIR CONDITIONING SMOKE QRH. COORD WITH PHX AND BASED ON THE SITUATION AND ACFT HISTORY THE L PACK WAS LEFT SHUT DOWN. NO SMOKE WAS SMELT AFTER THE L PACK WAS SHUT DOWN. THE PROBLEM BEING ISOLATED WE RETURNED TO PHX AND WENT INTO HOLDING TO BURN FUEL DOWN. DURING HOLDING WE ALSO NOTICED IN THE L CORNER OF THE CAPT'S FWD WINDOW THAT THERE HAD BEEN SOME ARCING AND SUSPECT THAT MAY HAVE ACTUALLY BEEN A CONTRIBUTING CAUSE.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.