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|
Attributes | |
ACN | 913601 |
Time | |
Date | 201010 |
Local Time Of Day | 0601-1200 |
Place | |
Locale Reference | ZOA.ARTCC |
State Reference | CA |
Aircraft 1 | |
Make Model Name | B777 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Component | |
Aircraft Component | Electrical Wiring & Connectors |
Person 1 | |
Function | Captain Pilot Not Flying |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 200 Flight Crew Total 20000 Flight Crew Type 5000 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Flight Deck / Cabin / Aircraft Event Smoke / Fire / Fumes / Odor |
Narrative:
Shortly after halfway point; and while climbing from FL360 to FL370; purser called cockpit and advised of a faint smoky smell near row 46. I initiated an ACARS message to maintenance control. Two or three minutes later; purser called back to say that the odor was much stronger. She informed me that no smoke was visible; but it was a strong smell. At this point; I turned off the ife/seat power and cabin utility switches; and also discontinued ACARS and called dispatch on the sat phone. I had dispatch patch through to maintenance control immediately. While talking to dispatch/maintenance control; purser notified me that the smell was lessened somewhat. At about the same time; a status message displayed bulk cargo ventilation fan. We did not know if this was because of the ife/cabin switches that we had turned off. Within a few more minutes; purser again notified us that the smell was worse. First officer and I quickly ran through the smoke procedures in the handbook; and turned off the recirc fans. While talking to maintenance control; we also turned off the gasper switch; and then the cargo heat switches. All this transpired in about 20 to maybe 30 minutes; and the smell eventually dissipated. We also had a firefighter in the cabin; who assisted the flight attendants in identifying the smoke/odor. The flight attendants thought it was electrical smelling; and this was confirmed by the firefighter. He suggested it could be electrical; or a rubber burning smell. With concurrence of maintenance control; we decided to leave the components off that we had turned off; for the remainder of the flight. Maintenance control also gave us a backup plan to go into the ee compartment to pull additional circuit breakers. We decided to do this only if the smoke returned. Dispatch advised ATC of our situation; but we decided to not declare an emergency at that time. The remainder of the flight was normal; with the exception of the passenger/galley/entertainment items that we had powered off. I did issue a cabin advisory to the purser; with a planned normal approach and landing. I gave a verbal briefing to the fam over the interphone. Dispatch; maintenance control; first officer; purser; fams and the firefighter all did an outstanding job. It was a very busy time for a bit; while trying to converse with dispatch/maintenance control/first officer/cabin and all; but we got everything done and covered I believe. The sat phone worked flawlessly. One area of confusion was the fact that there were numerous procedures for smoke problems; and it took a few extra minutes to go through those pages in the handbook. Since there was no visible smoke; it made it harder to isolate the problem area; while at the same time helped us in not having a real fire and associated passenger hysteria. I admit that my adrenaline was spiked some; but I believe we all did our required tasks to isolate the problem. Also; after landing; I did second guess myself with turning off the ife/cabin switches so rapidly; but after re-consideration; think it was proper and prudent. At this point I don't know if the smoke was from that bulk cargo ventilation fan; or something else; but being over 2 hours away from an airport; powering off the cabin items that we did was correct as well.
Original NASA ASRS Text
Title: B777 Captain was informed of a smoky smell in the cabin during an oceanic flight. Cabin electrical systems were deactivated then complied with handbook procedures and the smell dissipated.
Narrative: Shortly after halfway point; and while climbing from FL360 to FL370; Purser called cockpit and advised of a faint smoky smell near row 46. I initiated an ACARS message to Maintenance Control. Two or three minutes later; Purser called back to say that the odor was much stronger. She informed me that no smoke was visible; but it was a strong smell. At this point; I turned off the IFE/Seat power and Cabin Utility switches; and also discontinued ACARS and called Dispatch on the Sat Phone. I had Dispatch patch through to Maintenance Control immediately. While talking to Dispatch/Maintenance Control; Purser notified me that the smell was lessened somewhat. At about the same time; a status message displayed Bulk Cargo Ventilation Fan. We did not know if this was because of the IFE/Cabin switches that we had turned off. Within a few more minutes; Purser again notified us that the smell was worse. First Officer and I quickly ran through the smoke procedures in the handbook; and turned off the recirc fans. While talking to Maintenance Control; we also turned off the gasper switch; and then the cargo heat switches. All this transpired in about 20 to maybe 30 minutes; and the smell eventually dissipated. We also had a Firefighter in the cabin; who assisted the flight attendants in identifying the smoke/odor. The flight attendants thought it was electrical smelling; and this was confirmed by the firefighter. He suggested it could be electrical; or a rubber burning smell. With concurrence of Maintenance Control; we decided to leave the components off that we had turned off; for the remainder of the flight. Maintenance Control also gave us a backup plan to go into the EE compartment to pull additional circuit breakers. We decided to do this only if the smoke returned. Dispatch advised ATC of our situation; but we decided to not declare an emergency at that time. The remainder of the flight was normal; with the exception of the passenger/galley/entertainment items that we had powered off. I did issue a cabin advisory to the Purser; with a planned normal approach and landing. I gave a verbal briefing to the FAM over the interphone. Dispatch; Maintenance Control; First Officer; Purser; FAMs and the Firefighter all did an outstanding job. It was a very busy time for a bit; while trying to converse with Dispatch/Maintenance Control/First Officer/Cabin and all; but we got everything done and covered I believe. The Sat Phone worked flawlessly. One area of confusion was the fact that there were numerous procedures for smoke problems; and it took a few extra minutes to go through those pages in the Handbook. Since there was no visible smoke; it made it harder to isolate the problem area; while at the same time helped us in not having a real fire and associated passenger hysteria. I admit that my adrenaline was spiked some; but I believe we all did our required tasks to isolate the problem. Also; after landing; I did second guess myself with turning off the IFE/Cabin switches so rapidly; but after re-consideration; think it was proper and prudent. At this point I don't know if the smoke was from that Bulk Cargo Ventilation Fan; or something else; but being over 2 hours away from an airport; powering off the cabin items that we did was correct as well.
Data retrieved from NASA's ASRS site as of April 2012 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.