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|
Attributes | |
ACN | 93032 |
Time | |
Date | 198808 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : hgr |
State Reference | MD |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | ground : preflight ground other : taxi |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 5370 flight time type : 1781 |
ASRS Report | 93032 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | conflict : ground critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : anomaly accepted |
Consequence | faa : investigated |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation other |
Narrative:
I had just finished my regularly scheduled section at XA00PM. Flight control in dayton, oh, wanted me to call in. I called and they ask me to do an additional section. I requested not to due to an appointment with a surgeon my wife and I had made 2 1/2 weeks ago. I was having my parents in that day also from out of state and had only a short period to visit. Flight control told me that if I didn't fly the section I could look for another job. I reluctantly accepted what I could not change and had my wife cancel the appointment. My first officer then informed me he had taken ill and could not fly. Scheduling called in another first officer. 5 hours in aircraft and only 1 previous reposition flight. No regular flight duty. I went to the hangar and preflted the aircraft. Flight control did not get into phl by XB30 I would be getting home late and could not guarantee positive space home. Maintenance pulled aircraft out of hangar and did not check it or set brake. During my prestart checklist I set brake and held brakes at pedal for engine start. After starting #2 engine I requested gpu to be removed and start #1. After starting #1 and seeing ground personnel moving away to gpu I competed my flow and released parking brake. I did not have sufficient pressure on brakes to prevent aircraft from rolling 8' into gpu. Aircraft sustained damage to nose cone and minor damage to radar antenna. My head was in cockpit when aircraft started takeoff roll. First officer was new and was no help, but can't be blamed due to lack of experience. Many factors led to incident. Rush by company to get going time limits to prevent getting home late (as it was it was 13.7 hour day). Problems at home. New first officer. Fear of losing job if did not go. My being in too big a hurry. I will never be intimidated by company again.
Original NASA ASRS Text
Title: COMMUTER LTT ROLLED INTO GPU CAUSING DAMAGE TO ACFT.
Narrative: I HAD JUST FINISHED MY REGULARLY SCHEDULED SECTION AT XA00PM. FLT CTL IN DAYTON, OH, WANTED ME TO CALL IN. I CALLED AND THEY ASK ME TO DO AN ADDITIONAL SECTION. I REQUESTED NOT TO DUE TO AN APPOINTMENT WITH A SURGEON MY WIFE AND I HAD MADE 2 1/2 WKS AGO. I WAS HAVING MY PARENTS IN THAT DAY ALSO FROM OUT OF STATE AND HAD ONLY A SHORT PERIOD TO VISIT. FLT CTL TOLD ME THAT IF I DIDN'T FLY THE SECTION I COULD LOOK FOR ANOTHER JOB. I RELUCTANTLY ACCEPTED WHAT I COULD NOT CHANGE AND HAD MY WIFE CANCEL THE APPOINTMENT. MY F/O THEN INFORMED ME HE HAD TAKEN ILL AND COULD NOT FLY. SCHEDULING CALLED IN ANOTHER F/O. 5 HRS IN ACFT AND ONLY 1 PREVIOUS REPOSITION FLT. NO REGULAR FLT DUTY. I WENT TO THE HANGAR AND PREFLTED THE ACFT. FLT CTL DID NOT GET INTO PHL BY XB30 I WOULD BE GETTING HOME LATE AND COULD NOT GUARANTEE POSITIVE SPACE HOME. MAINT PULLED ACFT OUT OF HANGAR AND DID NOT CHK IT OR SET BRAKE. DURING MY PRESTART CHKLIST I SET BRAKE AND HELD BRAKES AT PEDAL FOR ENG START. AFTER STARTING #2 ENG I REQUESTED GPU TO BE REMOVED AND START #1. AFTER STARTING #1 AND SEEING GND PERSONNEL MOVING AWAY TO GPU I COMPETED MY FLOW AND RELEASED PARKING BRAKE. I DID NOT HAVE SUFFICIENT PRESSURE ON BRAKES TO PREVENT ACFT FROM ROLLING 8' INTO GPU. ACFT SUSTAINED DAMAGE TO NOSE CONE AND MINOR DAMAGE TO RADAR ANTENNA. MY HEAD WAS IN COCKPIT WHEN ACFT STARTED TKOF ROLL. F/O WAS NEW AND WAS NO HELP, BUT CAN'T BE BLAMED DUE TO LACK OF EXPERIENCE. MANY FACTORS LED TO INCIDENT. RUSH BY COMPANY TO GET GOING TIME LIMITS TO PREVENT GETTING HOME LATE (AS IT WAS IT WAS 13.7 HR DAY). PROBS AT HOME. NEW F/O. FEAR OF LOSING JOB IF DID NOT GO. MY BEING IN TOO BIG A HURRY. I WILL NEVER BE INTIMIDATED BY COMPANY AGAIN.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.