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|
Attributes | |
ACN | 94699 |
Time | |
Date | 198809 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : den |
State Reference | CO |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 19000 |
ASRS Report | 94699 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : flight engineer pilot : atp pilot : commercial |
Experience | flight time last 90 days : 210 flight time total : 5000 flight time type : 1400 |
ASRS Report | 94694 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | flight crew : declared emergency flight crew : rejected takeoff |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
It was necessary to abort takeoff due to engine #2 overtemp. The temperature of the engine was 940 degree at approximately takeoff speed of 130 KT. Improved takeoff climb was used due to airport condition and takeoff weight. Speeds were V1 153 vr 159 V2 162. Automatic braking was used for takeoff rejected takeoff position. After the aircraft came to a complete stop on the runway, the brakes overheated and 2 main gear tires were blown. I advised the tower of my disabled aircraft and requested assistance. Fire trucks came to the aircraft, followed by buses. Normal deplaning using stairs was completed west/O incident of any injuries.
Original NASA ASRS Text
Title: TKOF ABORTED DUE TO ENGINE OVERHEAT.
Narrative: IT WAS NECESSARY TO ABORT TKOF DUE TO ENG #2 OVERTEMP. THE TEMP OF THE ENG WAS 940 DEG AT APPROX TKOF SPD OF 130 KT. IMPROVED TKOF CLB WAS USED DUE TO ARPT CONDITION AND TKOF WT. SPDS WERE V1 153 VR 159 V2 162. AUTOMATIC BRAKING WAS USED FOR TKOF RTO POS. AFTER THE ACFT CAME TO A COMPLETE STOP ON THE RWY, THE BRAKES OVERHEATED AND 2 MAIN GEAR TIRES WERE BLOWN. I ADVISED THE TWR OF MY DISABLED ACFT AND REQUESTED ASSISTANCE. FIRE TRUCKS CAME TO THE ACFT, FOLLOWED BY BUSES. NORMAL DEPLANING USING STAIRS WAS COMPLETED W/O INCIDENT OF ANY INJURIES.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.