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|
Attributes | |
ACN | 95491 |
Time | |
Date | 198810 |
Day | Tue |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : mia |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Widebody, Low Wing, 3 Turbojet Eng |
Navigation In Use | Other |
Flight Phase | ground : parked |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 25000 flight time type : 4000 |
ASRS Report | 95491 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe aircraft equipment problem : critical other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | flight crew : declared emergency other |
Consequence | faa : investigated |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Engines were shut down and normal speed down and cool down. Securing checklist accomplished, APU inoperative since 9/fri/88. No ground air was connected. Ground electric was connected. I had left the aircraft. I was later informed that someone came onboard and reported a tailpipe fire in #2 engine. No air was available to rotate engine, which would be normal procedure, account inoperative APU. Cause of fire unknown to me. Fire was aggravated by lack of an APU--inoperative for 6 days. Corrective action recommended: better maintenance. Callback conversation with reporter revealed the following: confirmed #2 engine as the one of the tailpipe fire. All of crew had departed aircraft except captain who had delayed to go to head and when ground crew rushed on board to report fire, captain tried to motorize engine per procedure to put out fire, but with no air available account APU inoperative and ground air cart, although available not hooked up and running, was unable. Fire department arrived and put out fire. No further feedback on cause, but suspect pressurized fuel manifold leaked and vaporized into hot tailpipe. Did not think was damage to aircraft.
Original NASA ASRS Text
Title: ACR WDB HAS TAILPIPE FIRE AFTER SHUTDOWN AT GATE.
Narrative: ENGS WERE SHUT DOWN AND NORMAL SPD DOWN AND COOL DOWN. SECURING CHKLIST ACCOMPLISHED, APU INOP SINCE 9/FRI/88. NO GND AIR WAS CONNECTED. GND ELECTRIC WAS CONNECTED. I HAD LEFT THE ACFT. I WAS LATER INFORMED THAT SOMEONE CAME ONBOARD AND RPTED A TAILPIPE FIRE IN #2 ENG. NO AIR WAS AVAILABLE TO ROTATE ENG, WHICH WOULD BE NORMAL PROC, ACCOUNT INOP APU. CAUSE OF FIRE UNKNOWN TO ME. FIRE WAS AGGRAVATED BY LACK OF AN APU--INOP FOR 6 DAYS. CORRECTIVE ACTION RECOMMENDED: BETTER MAINT. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING: CONFIRMED #2 ENG AS THE ONE OF THE TAILPIPE FIRE. ALL OF CREW HAD DEPARTED ACFT EXCEPT CAPT WHO HAD DELAYED TO GO TO HEAD AND WHEN GND CREW RUSHED ON BOARD TO RPT FIRE, CAPT TRIED TO MOTORIZE ENG PER PROC TO PUT OUT FIRE, BUT WITH NO AIR AVAILABLE ACCOUNT APU INOP AND GND AIR CART, ALTHOUGH AVAILABLE NOT HOOKED UP AND RUNNING, WAS UNABLE. FIRE DEPT ARRIVED AND PUT OUT FIRE. NO FURTHER FEEDBACK ON CAUSE, BUT SUSPECT PRESSURIZED FUEL MANIFOLD LEAKED AND VAPORIZED INTO HOT TAILPIPE. DID NOT THINK WAS DAMAGE TO ACFT.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.