37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 96628 |
Time | |
Date | 198810 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : slc |
State Reference | UT |
Altitude | msl bound lower : 33000 msl bound upper : 33000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zlc artcc : zkc |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other |
Flight Phase | cruise other |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 7000 flight time type : 150 |
ASRS Report | 96628 |
Person 2 | |
Function | flight crew : captain |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Upon leveling at cruise, left fuel gauge dropped 600 pounds.--disconnected autopilot, a/C appeared in balance. Put aircraft back on autopilot, right gauge dropped 3000+ pounds to around 1500. Stayed down 2-3 min, then started fluctuating. Took fuel slip, and found the gallons total, converted to pounds, added to block in fuel of previous flight did not match gauges, fuel slip, or flight plan. All three matched at T/O. As the aircraft had 2 previous write ups for gauges reading high, not low, elected to divert to slc, the nearest suitable airport, as it was within gliding distance. Maintenance should have fixed this the first time! On the ground, the a/C was dripsticked, and the gauges came up to match. After maintenance signed off, the a/C was topped off, redripped, and ferried to our maintenance base with a mechanic on the jump seat. In-flight, he observed the same problems as the previous flight.
Original NASA ASRS Text
Title: FUEL GAUGE PROBLEM, READING LOW.
Narrative: UPON LEVELING AT CRUISE, LEFT FUEL GAUGE DROPPED 600 LBS.--DISCONNECTED AUTOPILOT, A/C APPEARED IN BALANCE. PUT ACFT BACK ON AUTOPILOT, RIGHT GAUGE DROPPED 3000+ LBS TO AROUND 1500. STAYED DOWN 2-3 MIN, THEN STARTED FLUCTUATING. TOOK FUEL SLIP, AND FOUND THE GALLONS TOTAL, CONVERTED TO LBS, ADDED TO BLOCK IN FUEL OF PREVIOUS FLIGHT DID NOT MATCH GAUGES, FUEL SLIP, OR FLIGHT PLAN. ALL THREE MATCHED AT T/O. AS THE ACFT HAD 2 PREVIOUS WRITE UPS FOR GAUGES READING HIGH, NOT LOW, ELECTED TO DIVERT TO SLC, THE NEAREST SUITABLE AIRPORT, AS IT WAS WITHIN GLIDING DISTANCE. MAINT SHOULD HAVE FIXED THIS THE FIRST TIME! ON THE GND, THE A/C WAS DRIPSTICKED, AND THE GAUGES CAME UP TO MATCH. AFTER MAINT SIGNED OFF, THE A/C WAS TOPPED OFF, REDRIPPED, AND FERRIED TO OUR MAINT BASE WITH A MECHANIC ON THE JUMP SEAT. INFLT, HE OBSERVED THE SAME PROBLEMS AS THE PREVIOUS FLIGHT.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.