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|
Attributes | |
ACN | 99753 |
Time | |
Date | 198812 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : sdf |
State Reference | KY |
Altitude | msl bound lower : 7000 msl bound upper : 7000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : sdfg |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : commercial pilot : atp pilot : instrument |
Experience | flight time last 90 days : 180 flight time total : 14000 flight time type : 4500 |
ASRS Report | 99753 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : instrument pilot : commercial pilot : flight engineer pilot : atp pilot : cfi |
Experience | flight time last 90 days : 171 flight time total : 4400 flight time type : 307 |
ASRS Report | 99945 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far |
Independent Detector | other flight crewa |
Resolutory Action | none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Approximately 7000' on climb out from sdf #2 oil filter bypass light came on after reducing thrust (per procedure), light stayed on, engine was shutdown. I considered it a safer course of action to continue to ord because of airport facs and runway selections (WX was good for entire route of flight, performance wasn't a problem because of light weight). I feel captain should have more leeway in decision making in 3 or 4 engine jets than FAA currently gives in engine shutdown cases.
Original NASA ASRS Text
Title: ENGINE FAILED SHORTLY AFTER TKOF AND CREW DECIDED TO FLY TO DESTINATION.
Narrative: APPROX 7000' ON CLBOUT FROM SDF #2 OIL FILTER BYPASS LIGHT CAME ON AFTER REDUCING THRUST (PER PROC), LIGHT STAYED ON, ENG WAS SHUTDOWN. I CONSIDERED IT A SAFER COURSE OF ACTION TO CONTINUE TO ORD BECAUSE OF ARPT FACS AND RWY SELECTIONS (WX WAS GOOD FOR ENTIRE ROUTE OF FLT, PERFORMANCE WASN'T A PROB BECAUSE OF LIGHT WEIGHT). I FEEL CAPT SHOULD HAVE MORE LEEWAY IN DECISION MAKING IN 3 OR 4 ENG JETS THAN FAA CURRENTLY GIVES IN ENG SHUTDOWN CASES.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.