Narrative:

At FL350, the #1 engine seized west/O any warning. We were approximately 2 hours and 20 mins into the flight. Emergency action. Ignition override. Gave no results, engine shutdown procedure followed. (We made an uneventful landing in las.) we declared emergency and requested lower altitude immediately. We received clearance to descend to FL240 and later to 1000' MSL. When electrical shifted to the #2 engine after the #1 engine failed, and again when it shifted to the APU once the APU was started, the #2 engine surged. The #1 engine had been previously written up on a previous flight having an oil filter screen clogged. It was checked in jackson, mi, and signed off. The flight from jackson, mi, to dfw was uneventful. Our flight was dfw to sjc.

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Original NASA ASRS Text

Title: ACR MLG EXPERIENCES ENGINE FAILURE AT CRUISE.

Narrative: AT FL350, THE #1 ENG SEIZED W/O ANY WARNING. WE WERE APPROX 2 HRS AND 20 MINS INTO THE FLT. EMER ACTION. IGNITION OVERRIDE. GAVE NO RESULTS, ENG SHUTDOWN PROC FOLLOWED. (WE MADE AN UNEVENTFUL LNDG IN LAS.) WE DECLARED EMER AND REQUESTED LOWER ALT IMMEDIATELY. WE RECEIVED CLRNC TO DSND TO FL240 AND LATER TO 1000' MSL. WHEN ELECTRICAL SHIFTED TO THE #2 ENG AFTER THE #1 ENG FAILED, AND AGAIN WHEN IT SHIFTED TO THE APU ONCE THE APU WAS STARTED, THE #2 ENG SURGED. THE #1 ENG HAD BEEN PREVIOUSLY WRITTEN UP ON A PREVIOUS FLT HAVING AN OIL FILTER SCREEN CLOGGED. IT WAS CHKED IN JACKSON, MI, AND SIGNED OFF. THE FLT FROM JACKSON, MI, TO DFW WAS UNEVENTFUL. OUR FLT WAS DFW TO SJC.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.