37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 208649 |
Time | |
Date | 199204 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : yxu |
State Reference | ON |
Altitude | msl bound lower : 26000 msl bound upper : 26000 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | cruise other |
Route In Use | enroute airway : czyz |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 24300 flight time type : 12500 |
ASRS Report | 208649 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 200 flight time total : 9000 flight time type : 5000 |
ASRS Report | 208892 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | controller : issued new clearance flight crew : overcame equipment problem flight crew : declared emergency |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
In level flight lost right hydraulic system. Apparently, the main landing gear came part way out and caused extreme drag. Performed emergency procedure and notified company maintenance and dispatch. All agreed that with fuel burn rate and remaining fuel on board, we would not be able to make destination. We then diverted to london, on and made a safe and normal landing. The company has cut back the amount of fuel carried on most segments as a cost-saving measure. This combined with a long taxi delay from the departure station, left very little room for unforeseen circumstances.
Original NASA ASRS Text
Title: AN ACR MLG CREW HAD A HYD LEAK IN FLT. THEY LANDED SAFELY WITHOUT DAMAGE OR INJURY AT AN ENRTE ARPT. THE ENRTE LNDG WAS MADE BECAUSE OF SUSPECTED HIGH FUEL FLOW BECAUSE OF HIGH DRAG.
Narrative: IN LEVEL FLT LOST R HYD SYS. APPARENTLY, THE MAIN LNDG GEAR CAME PART WAY OUT AND CAUSED EXTREME DRAG. PERFORMED EMER PROC AND NOTIFIED COMPANY MAINT AND DISPATCH. ALL AGREED THAT WITH FUEL BURN RATE AND REMAINING FUEL ON BOARD, WE WOULD NOT BE ABLE TO MAKE DEST. WE THEN DIVERTED TO LONDON, ON AND MADE A SAFE AND NORMAL LNDG. THE COMPANY HAS CUT BACK THE AMOUNT OF FUEL CARRIED ON MOST SEGMENTS AS A COST-SAVING MEASURE. THIS COMBINED WITH A LONG TAXI DELAY FROM THE DEP STATION, LEFT VERY LITTLE ROOM FOR UNFORESEEN CIRCUMSTANCES.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.