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|
Attributes | |
ACN | 210886 |
Time | |
Date | 199205 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : sby |
State Reference | MD |
Altitude | msl bound lower : 29000 msl bound upper : 31000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zdc tower : rdu |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | climbout : intermediate altitude cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 225 flight time total : 4800 flight time type : 500 |
ASRS Report | 210886 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
While climbing through FL290 to FL350, fluctuating fuel flow and EPR observed on #2 engine followed by compressor stall on #2 engine. Power was reduced and climb was stopped. Requested and received clearance to FL280. We ran abnormal procedure for compressor stall in flight and engine performance was normal. Elected to continue en route via inland route to mia in case of future problems with engine. We also climbed to FL310 for final cruise altitude. En route flight engineer observed he was unable to xfeed fuel from #1 tank. We monitored situation and fuel never became unbalanced. Landing was uneventful in mia. Mia maintenance discovered #1 xfeed valve knob was installed backwards. In hindsight, compressor stall was probably caused by lack of positive fuel pressure to engine caused by backward xfeed knob. After performing abnormal procedure and after climbing to FL310 with no abnormal indications, I felt engine was reliable and it was safe to proceed to destination, but in the remote chance that we did have a future problem with the engine, we chose the inland route as the safest alternative.
Original NASA ASRS Text
Title: ACFT EQUIP PROBLEM MANDATES A RERTE AND LOWER FLT ALT TO DEST ARPT.
Narrative: WHILE CLBING THROUGH FL290 TO FL350, FLUCTUATING FUEL FLOW AND EPR OBSERVED ON #2 ENG FOLLOWED BY COMPRESSOR STALL ON #2 ENG. PWR WAS REDUCED AND CLB WAS STOPPED. REQUESTED AND RECEIVED CLRNC TO FL280. WE RAN ABNORMAL PROC FOR COMPRESSOR STALL IN FLT AND ENG PERFORMANCE WAS NORMAL. ELECTED TO CONTINUE ENRTE VIA INLAND RTE TO MIA IN CASE OF FUTURE PROBLEMS WITH ENG. WE ALSO CLBED TO FL310 FOR FINAL CRUISE ALT. ENRTE FLT ENGINEER OBSERVED HE WAS UNABLE TO XFEED FUEL FROM #1 TANK. WE MONITORED SITUATION AND FUEL NEVER BECAME UNBALANCED. LNDG WAS UNEVENTFUL IN MIA. MIA MAINT DISCOVERED #1 XFEED VALVE KNOB WAS INSTALLED BACKWARDS. IN HINDSIGHT, COMPRESSOR STALL WAS PROBABLY CAUSED BY LACK OF POSITIVE FUEL PRESSURE TO ENG CAUSED BY BACKWARD XFEED KNOB. AFTER PERFORMING ABNORMAL PROC AND AFTER CLBING TO FL310 WITH NO ABNORMAL INDICATIONS, I FELT ENG WAS RELIABLE AND IT WAS SAFE TO PROCEED TO DEST, BUT IN THE REMOTE CHANCE THAT WE DID HAVE A FUTURE PROBLEM WITH THE ENG, WE CHOSE THE INLAND RTE AS THE SAFEST ALTERNATIVE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.