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|
Attributes | |
ACN | 238983 |
Time | |
Date | 199303 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : phx |
State Reference | AZ |
Altitude | msl bound lower : 2000 msl bound upper : 2000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : phx tower : san |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | cruise other descent other landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 4200 flight time type : 2500 |
ASRS Report | 238983 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other controllera other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Noticed higher than normal fuel consumption at cruise altitude. Was feeding all fuel out of tank #2. Departed with all tanks topped off. Went to tank to engine. Determined #2 tank was being depleted more quickly than 1 or 3. All engine parameters normal. Continued to destination. Upon contacting tower, they stated it looked like smoke coming out of engine #2. No fire warn no abnormal engine gauge reading. Called for fire equipment. Upon landing, taxied off active, shut down engine #2, pulled away from other aircraft/buildings. No fire. Taxied to gate after lengthy delay due to not being able to talk to fire equipment from cockpit. Upon shutdown maintenance found fuel control seal broken. The 'smoke' was fuel vaporizing and running under engine cowling. Should have throttled back and maybe shut down #2 engine to be sure fuel leak was stopped. Low fuel was not a problem since we topped off at departure airport.
Original NASA ASRS Text
Title: FUEL LEAK OF MLG ACR ACFT ON FINAL CAUSED TWR TO RPT SMOKE FROM THE ACFT RESULTING IN EMER GND EQUIP TO MEET ACFT AFTER LNDG.
Narrative: NOTICED HIGHER THAN NORMAL FUEL CONSUMPTION AT CRUISE ALT. WAS FEEDING ALL FUEL OUT OF TANK #2. DEPARTED WITH ALL TANKS TOPPED OFF. WENT TO TANK TO ENG. DETERMINED #2 TANK WAS BEING DEPLETED MORE QUICKLY THAN 1 OR 3. ALL ENG PARAMETERS NORMAL. CONTINUED TO DEST. UPON CONTACTING TWR, THEY STATED IT LOOKED LIKE SMOKE COMING OUT OF ENG #2. NO FIRE WARN NO ABNORMAL ENG GAUGE READING. CALLED FOR FIRE EQUIP. UPON LNDG, TAXIED OFF ACTIVE, SHUT DOWN ENG #2, PULLED AWAY FROM OTHER ACFT/BUILDINGS. NO FIRE. TAXIED TO GATE AFTER LENGTHY DELAY DUE TO NOT BEING ABLE TO TALK TO FIRE EQUIP FROM COCKPIT. UPON SHUTDOWN MAINT FOUND FUEL CTL SEAL BROKEN. THE 'SMOKE' WAS FUEL VAPORIZING AND RUNNING UNDER ENG COWLING. SHOULD HAVE THROTTLED BACK AND MAYBE SHUT DOWN #2 ENG TO BE SURE FUEL LEAK WAS STOPPED. LOW FUEL WAS NOT A PROB SINCE WE TOPPED OFF AT DEP ARPT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.