37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 247700 |
Time | |
Date | 199307 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : gcm |
State Reference | FO |
Altitude | msl bound lower : 2500 msl bound upper : 2500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : gcm artcc : zse |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : intermediate altitude |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 247700 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : flight engineer pilot : atp pilot : cfi |
Experience | flight time last 90 days : 150 flight time total : 11000 flight time type : 2000 |
ASRS Report | 247804 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other other : unspecified |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
At approximately 2500 ft, a flight attendant reported a louder than normal noise coming from area over right wing emergency exit. We confirmed that the cabin was climbing with the aircraft and initiated a slow descent and normal landing back at grand cayman. Ground personnel confirmed the over wing exit hatch was not seated properly. It was reseated and the flight was continued with another takeoff without further difficulty. The hatch was not noticeably loose by visual inspection prior to the first takeoff.
Original NASA ASRS Text
Title: ACFT EQUIP PROB MANDATES A RETURN AND LAND TO RESEAT OVER WING PAX EXIT.
Narrative: AT APPROX 2500 FT, A FLT ATTENDANT RPTED A LOUDER THAN NORMAL NOISE COMING FROM AREA OVER R WING EMER EXIT. WE CONFIRMED THAT THE CABIN WAS CLBING WITH THE ACFT AND INITIATED A SLOW DSCNT AND NORMAL LNDG BACK AT GRAND CAYMAN. GND PERSONNEL CONFIRMED THE OVER WING EXIT HATCH WAS NOT SEATED PROPERLY. IT WAS RESEATED AND THE FLT WAS CONTINUED WITH ANOTHER TKOF WITHOUT FURTHER DIFFICULTY. THE HATCH WAS NOT NOTICEABLY LOOSE BY VISUAL INSPECTION PRIOR TO THE FIRST TKOF.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.