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Attributes | |
ACN | 250673 |
Time | |
Date | 199309 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : sdf |
State Reference | KY |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : rfd |
Operator | general aviation : corporate |
Make Model Name | Light Transport |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : commercial pilot : atp pilot : instrument |
Experience | flight time last 90 days : 36 flight time total : 10748 flight time type : 2066 |
ASRS Report | 250673 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 24 flight time total : 405 flight time type : 77 |
ASRS Report | 250746 |
Events | |
Anomaly | aircraft equipment problem : critical conflict : ground critical other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
This occurrence involves the light transport freighter, a chartered flight to raleigh county memorial field, beckley, wv. All pre takeoff procedures were completed and the flight was cleared to depart runway 19 standiford. At this stage no abnormalities or discrepancies were noted by the flight crew. Takeoff power was applied by myself and monitored by the copilot, per company SOP. The procedure for takeoff was standard, rotate at 84 KTS, flaps up, outside conditions were cool and VMC, dry surface with calm winds. I remember no aircraft departing prior to us. Operations were normal until 75-80 KTS. At this speed the left wing very abruptly rose and the aircraft started to veer to the right. I immediately countered this by applying left rudder in an effort to maintain centerline tracking. At this point I decided to abort the takeoff due to an unknown problem. A lateral oscillation ensued which was subsequently impossible to control and the aircraft departed the runway to the left. The area to the left of the runway was grassed and had standard flight markings in place. Braking and directional control were difficult due to wet grass (from dew) and the aircraft's high speed. Trying to evade obstacles was attempted, but regrettably a runway distance marker and taxiway light were hit. By the time the aircraft reached runway 11/29 I had regained sufficient control to taxi the aircraft to a side taxiway stub, cut engines and stopped the aircraft. I ordered the copilot to assist in the visual inspection. I remained aboard the aircraft. The crew reported damage of a 20-inch tear to the left outboard flap, and a tear of 4-5 inches in the fabric on the left elevator. The flap damage appeared to be consistent with an impact on a runway distance marker and the elevator damage with a runway light. The flap was also seen to be hanging approximately 2 inches below the other flaps. Otherwise, no further damage to the aircraft or injuries to the crew were reported. Landing gear lock pins were positioned and the aircraft was taxied back to the west ramp. I am unable to ascertain the reason for this incident. Both engines were able to start for the return taxi to the ups rammp, no wind gusts or wake turbulence was reported. All aircraft system seemed to be operating normally prior to the excursion. Supplemental information from acn 250746: upon reanalyzing the events during the takeoff roll, we (the flight crew) feel that if the left outboard flap had been drooping during the takeoff roll, there would have been adequate asymmetrical forces to make the aircraft difficult to control. All checklist procedures were completed as required and the flaps had been cycled, retracted, and indicating normal prior to the takeoff roll. However, since you cannot see the flaps and their condition from the pilot seats, there is no way to determine whether there was a flap 'droop' on the takeoff roll.
Original NASA ASRS Text
Title: ACFT DAMAGED ON TKOF ABORT EFFORT WHICH HAD TURNED INTO A RWY EXCURSION.
Narrative: THIS OCCURRENCE INVOLVES THE LTT FREIGHTER, A CHARTERED FLT TO RALEIGH COUNTY MEMORIAL FIELD, BECKLEY, WV. ALL PRE TKOF PROCS WERE COMPLETED AND THE FLT WAS CLRED TO DEPART RWY 19 STANDIFORD. AT THIS STAGE NO ABNORMALITIES OR DISCREPANCIES WERE NOTED BY THE FLC. TKOF PWR WAS APPLIED BY MYSELF AND MONITORED BY THE COPLT, PER COMPANY SOP. THE PROC FOR TKOF WAS STANDARD, ROTATE AT 84 KTS, FLAPS UP, OUTSIDE CONDITIONS WERE COOL AND VMC, DRY SURFACE WITH CALM WINDS. I REMEMBER NO ACFT DEPARTING PRIOR TO US. OPS WERE NORMAL UNTIL 75-80 KTS. AT THIS SPD THE L WING VERY ABRUPTLY ROSE AND THE ACFT STARTED TO VEER TO THE R. I IMMEDIATELY COUNTERED THIS BY APPLYING L RUDDER IN AN EFFORT TO MAINTAIN CTRLINE TRACKING. AT THIS POINT I DECIDED TO ABORT THE TKOF DUE TO AN UNKNOWN PROB. A LATERAL OSCILLATION ENSUED WHICH WAS SUBSEQUENTLY IMPOSSIBLE TO CTL AND THE ACFT DEPARTED THE RWY TO THE L. THE AREA TO THE L OF THE RWY WAS GRASSED AND HAD STANDARD FLT MARKINGS IN PLACE. BRAKING AND DIRECTIONAL CTL WERE DIFFICULT DUE TO WET GRASS (FROM DEW) AND THE ACFT'S HIGH SPD. TRYING TO EVADE OBSTACLES WAS ATTEMPTED, BUT REGRETTABLY A RWY DISTANCE MARKER AND TXWY LIGHT WERE HIT. BY THE TIME THE ACFT REACHED RWY 11/29 I HAD REGAINED SUFFICIENT CTL TO TAXI THE ACFT TO A SIDE TXWY STUB, CUT ENGS AND STOPPED THE ACFT. I ORDERED THE COPLT TO ASSIST IN THE VISUAL INSPECTION. I REMAINED ABOARD THE ACFT. THE CREW RPTED DAMAGE OF A 20-INCH TEAR TO THE L OUTBOARD FLAP, AND A TEAR OF 4-5 INCHES IN THE FABRIC ON THE L ELEVATOR. THE FLAP DAMAGE APPEARED TO BE CONSISTENT WITH AN IMPACT ON A RWY DISTANCE MARKER AND THE ELEVATOR DAMAGE WITH A RWY LIGHT. THE FLAP WAS ALSO SEEN TO BE HANGING APPROX 2 INCHES BELOW THE OTHER FLAPS. OTHERWISE, NO FURTHER DAMAGE TO THE ACFT OR INJURIES TO THE CREW WERE RPTED. LNDG GEAR LOCK PINS WERE POSITIONED AND THE ACFT WAS TAXIED BACK TO THE W RAMP. I AM UNABLE TO ASCERTAIN THE REASON FOR THIS INCIDENT. BOTH ENGS WERE ABLE TO START FOR THE RETURN TAXI TO THE UPS RAMMP, NO WIND GUSTS OR WAKE TURB WAS RPTED. ALL ACFT SYS SEEMED TO BE OPERATING NORMALLY PRIOR TO THE EXCURSION. SUPPLEMENTAL INFO FROM ACN 250746: UPON REANALYZING THE EVENTS DURING THE TKOF ROLL, WE (THE FLC) FEEL THAT IF THE L OUTBOARD FLAP HAD BEEN DROOPING DURING THE TKOF ROLL, THERE WOULD HAVE BEEN ADEQUATE ASYMMETRICAL FORCES TO MAKE THE ACFT DIFFICULT TO CTL. ALL CHKLIST PROCS WERE COMPLETED AS REQUIRED AND THE FLAPS HAD BEEN CYCLED, RETRACTED, AND INDICATING NORMAL PRIOR TO THE TKOF ROLL. HOWEVER, SINCE YOU CANNOT SEE THE FLAPS AND THEIR CONDITION FROM THE PLT SEATS, THERE IS NO WAY TO DETERMINE WHETHER THERE WAS A FLAP 'DROOP' ON THE TKOF ROLL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.