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|
Attributes | |
ACN | 252755 |
Time | |
Date | 199309 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dca |
State Reference | DC |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : atp pilot : commercial |
Experience | flight time last 90 days : 240 flight time total : 24000 flight time type : 5000 |
ASRS Report | 252755 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 150 flight time total : 8500 |
ASRS Report | 253488 |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
I proceeded with my cockpit checks. Everything checked normal. I then left cockpit for a short while. When I returned and seated in my seat I rested my feet on the rudder pedals. I noticed my left foot was further in than the right. I reached up and turned on hydraulic pump thinking that jet blast or surface wind caused rudder displacement. This did not correct situation. About then, we were readying for pushback and engine start. After engine start and all hydraulic pumps turned on, rudder displacement did not change. It was then I rechked rudder trim and found it to be 10 degrees left. Cause of this is undetermined. Callback conversation with reporter revealed the following information: the reporting captain has no new notions as to what may have happened here, unless a window cleaner may have kicked the trim handle. The captain was not in the cockpit the whole time. He has not seen or heard of this happening again.
Original NASA ASRS Text
Title: AN ACR MLG CREW FOUND THAT ITS RUDDER TRIM SEEMED TO HAVE CHANGED 10 UNITS BY ITSELF.
Narrative: I PROCEEDED WITH MY COCKPIT CHKS. EVERYTHING CHKED NORMAL. I THEN LEFT COCKPIT FOR A SHORT WHILE. WHEN I RETURNED AND SEATED IN MY SEAT I RESTED MY FEET ON THE RUDDER PEDALS. I NOTICED MY L FOOT WAS FURTHER IN THAN THE R. I REACHED UP AND TURNED ON HYD PUMP THINKING THAT JET BLAST OR SURFACE WIND CAUSED RUDDER DISPLACEMENT. THIS DID NOT CORRECT SIT. ABOUT THEN, WE WERE READYING FOR PUSHBACK AND ENG START. AFTER ENG START AND ALL HYD PUMPS TURNED ON, RUDDER DISPLACEMENT DID NOT CHANGE. IT WAS THEN I RECHKED RUDDER TRIM AND FOUND IT TO BE 10 DEGS L. CAUSE OF THIS IS UNDETERMINED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTING CAPT HAS NO NEW NOTIONS AS TO WHAT MAY HAVE HAPPENED HERE, UNLESS A WINDOW CLEANER MAY HAVE KICKED THE TRIM HANDLE. THE CAPT WAS NOT IN THE COCKPIT THE WHOLE TIME. HE HAS NOT SEEN OR HEARD OF THIS HAPPENING AGAIN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.