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|
Attributes | |
ACN | 265831 |
Time | |
Date | 199403 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : alb |
State Reference | NY |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : orf |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time total : 6900 flight time type : 1200 |
ASRS Report | 265831 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : flight engineer pilot : private pilot : instrument |
Experience | flight time last 90 days : 180 flight time total : 5700 flight time type : 180 |
ASRS Report | 265705 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : rejected takeoff none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Takeoff aborted due to compressor stalls as airspeed approached 60 KTS. After clearing the runway and checking all instruments, it was thought that stalls may have occurred due to gusting crosswind as all engine parameters were normal. Second takeoff was initiated but not attempted as #1 engine started compressor stalling as power was advanced. After taxiing back to gate, it was discovered that the engine hub (bullet) had come unbolted and was lying at the bottom of engine nacelle.
Original NASA ASRS Text
Title: AN ACR B-727 ABORTED ITS TKOF.
Narrative: TKOF ABORTED DUE TO COMPRESSOR STALLS AS AIRSPD APCHED 60 KTS. AFTER CLRING THE RWY AND CHKING ALL INSTS, IT WAS THOUGHT THAT STALLS MAY HAVE OCCURRED DUE TO GUSTING XWIND AS ALL ENG PARAMETERS WERE NORMAL. SECOND TKOF WAS INITIATED BUT NOT ATTEMPTED AS #1 ENG STARTED COMPRESSOR STALLING AS PWR WAS ADVANCED. AFTER TAXIING BACK TO GATE, IT WAS DISCOVERED THAT THE ENG HUB (BULLET) HAD COME UNBOLTED AND WAS LYING AT THE BOTTOM OF ENG NACELLE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.