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|
Attributes | |
ACN | 268246 |
Time | |
Date | 199404 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : cmk airport : hpn |
State Reference | NY |
Altitude | msl bound lower : 7000 msl bound upper : 7000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : lga |
Operator | general aviation : personal |
Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise other other |
Route In Use | enroute airway : n90 |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 11 flight time total : 950 flight time type : 100 |
ASRS Report | 268246 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Flight on previous day (orh to teb) was VFR and uneventful. Return to orh was IFR. Run-up and climb were normal. After leveling at 7000 ft AGL, radios faded. A check of system revealed `altitude' circuit breaker had tripped. It was reset, radio contact was reestablished and controller reported radar transponder was not being received. Transponder was reset and worked. A short time later, circuit breaker tripped again and was reset. At this point, burning insulation was smelled in the cockpit by both pilot and passenger. The `altitude' circuit breaker was opened and landing at the nearest airport was requested. Pilot used own navigation and made ILS 16 approach at hpn without incident. The aircraft was taxied to a service facility. Alternator windings had fused and rotor was worn where brushes made contact. The alternator and voltage regulator were replaced, as was the master switch. However, a positive reading on the ammeter is still not present and maintenance is continuing to trouble- shoot the problem.
Original NASA ASRS Text
Title: ELECTRICAL SYS FAILURE DUE TO ALTERNATOR, VOLTAGE REGULATOR FAILURE.
Narrative: FLT ON PREVIOUS DAY (ORH TO TEB) WAS VFR AND UNEVENTFUL. RETURN TO ORH WAS IFR. RUN-UP AND CLB WERE NORMAL. AFTER LEVELING AT 7000 FT AGL, RADIOS FADED. A CHK OF SYS REVEALED `ALT' CIRCUIT BREAKER HAD TRIPPED. IT WAS RESET, RADIO CONTACT WAS REESTABLISHED AND CTLR RPTED RADAR XPONDER WAS NOT BEING RECEIVED. XPONDER WAS RESET AND WORKED. A SHORT TIME LATER, CIRCUIT BREAKER TRIPPED AGAIN AND WAS RESET. AT THIS POINT, BURNING INSULATION WAS SMELLED IN THE COCKPIT BY BOTH PLT AND PAX. THE `ALT' CIRCUIT BREAKER WAS OPENED AND LNDG AT THE NEAREST ARPT WAS REQUESTED. PLT USED OWN NAV AND MADE ILS 16 APCH AT HPN WITHOUT INCIDENT. THE ACFT WAS TAXIED TO A SVC FACILITY. ALTERNATOR WINDINGS HAD FUSED AND ROTOR WAS WORN WHERE BRUSHES MADE CONTACT. THE ALTERNATOR AND VOLTAGE REGULATOR WERE REPLACED, AS WAS THE MASTER SWITCH. HOWEVER, A POSITIVE READING ON THE AMMETER IS STILL NOT PRESENT AND MAINT IS CONTINUING TO TROUBLE- SHOOT THE PROB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.