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|
Attributes | |
ACN | 294124 |
Time | |
Date | 199501 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : pit |
State Reference | PA |
Altitude | msl bound lower : 5000 msl bound upper : 5000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : pit tracon : cvg |
Operator | common carrier : air carrier |
Make Model Name | Fokker 100 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : initial climbout : intermediate altitude other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 12000 flight time type : 2000 |
ASRS Report | 294124 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 210 flight time total : 14000 flight time type : 450 |
ASRS Report | 294375 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other other |
Consequence | faa : reviewed incident with flight crew Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Shortly after takeoff, we experienced a loss of hydraulic quantity on the #2 hydraulic system. Shut off #2 engine pumps as per procedure, ran appropriate checklists, and returned to land at pit. Approach and landing were without incident but workload was increased by repeated interruptions from ATC. Finally had to resort to the 'don't call us, we'll call you' method until we were ready for landing. Maintenance found hydraulic supply hose fitting loose.
Original NASA ASRS Text
Title: FLC OF AN MLG RETURNED AFTER TKOF DUE TO LOSS OF HYD FLUID QUANTITY.
Narrative: SHORTLY AFTER TKOF, WE EXPERIENCED A LOSS OF HYD QUANTITY ON THE #2 HYD SYS. SHUT OFF #2 ENG PUMPS AS PER PROC, RAN APPROPRIATE CHKLISTS, AND RETURNED TO LAND AT PIT. APCH AND LNDG WERE WITHOUT INCIDENT BUT WORKLOAD WAS INCREASED BY REPEATED INTERRUPTIONS FROM ATC. FINALLY HAD TO RESORT TO THE 'DON'T CALL US, WE'LL CALL YOU' METHOD UNTIL WE WERE READY FOR LNDG. MAINT FOUND HYD SUPPLY HOSE FITTING LOOSE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.